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THROUGH TUBING SAND CONTROL WITH VENT SCREEN

机译:通过通风孔通过沙管控制

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Following excessive sand production from the HB-1 Well in the Bekapai Field, the oil production from the central panel of the main zone was stopped. A cost-effective sand control solution was needed to reproduce that zone since Bekapai field is a mature field with mediocre gain expected. This solution will have to overcome several challenges which are: 1. Through tubing operation with an old completion (more than 20 years old) with a very small ID. 2. Dual annulus configuration: sand control solution to be applied in a concentric configuration of 5"1/2 blank pipe inside a 9"5/8 casing. 3. Small tripod platform: lifting and handling operation directly from crane barge due to limited working space. The solution chosen was to utilize a Vent screen combined with a high rate water pack. This method is a compromise between an expensive frac-pack operation and a low productivity classic gravel pack operation. The Vent Screen method uses two screen assemblies separated by blank pipe (Figure 2). Proppant is packed around the lower screen and most of the blank pipe. The differential pressure created on the screen annulus will create a unique flow path. The high rate water pack is aiming to by-pass only the damaging zone in the near wellbore to maximize productivity. The job design objective was to optimize productivity through the vent screen by an enhanced design of the perforation and pumping method. Prior to starting the job, a tubing wash and a sand cleaning were performed. Dual wire wrapped screens were deployed with a Coil Tubing Unit and set on top of the plug covered by cement. A high rate water pack treatment was performed by pumping the proppant using VES (Visco Elastic Surfactant) carrier fluid. After Nitrogen off-load, the well was able to produce oil at the same production rate as before shut in and without any sand trace or proppant flow back indication on surface. The break even point was reached after less than 5 months. This paper will discuss the design method, job execution and lessons learned from this operation.
机译:在Bekapai油田的HB-1井中产生过多的沙子后,该主区中部的石油停止生产。由于Bekapai油田是一个成熟的油田,预期收益平平,因此需要一种经济有效的防砂解决方案来重现该地区。该解决方案将必须克服以下几个挑战:1.通过具有很小内径的旧完井(超过20年)的油管作业。 2.双环面配置:防砂解决方案将在9“ 5/8套管内的5” 1/2空白管的同心配置中应用。 3.小型三脚架平台:由于工作空间有限,可直接从起重机驳船进行举升和搬运操作。选择的解决方案是结合使用通风筛网和高速率水包。这种方法是在昂贵的压裂填充操作和低生产率的传统砾石填充操作之间进行折衷。排气筛方法使用两个由空管分隔的筛组件(图2)。支撑剂包装在下部筛网和大部分空白管周围。在筛环上产生的压差将产生独特的流动路径。高流量水包旨在仅绕过井眼附近的损坏区域,以最大化生产率。工作设计的目标是通过穿孔和泵送方法的增强设计来优化通气孔的生产率。在开始工作之前,先进行油管清洗和沙石清洗。将双绕线屏蔽与线圈管单元一起部署,并置于由水泥覆盖的塞子顶部。通过使用VES(粘弹性表面活性剂)载液泵送支撑剂来进行高速率水包处理。氮气卸荷后,该井能够以与关闭之前相同的生产率生产油,并且在地面上没有任何沙迹或支撑剂回流的迹象。不到5个月后就达到了收支平衡点。本文将讨论设计方法,作业执行以及从此操作中学到的经验教训。

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