首页> 外文会议>American Institute of Mining, Metallurgical and Petroleum Engineers;American Institute of Chemical Engineers;American Association of Petroleum Geologists;Offshore Technology Conference >Optimizations and Tubular Practice from Integrated Packer Stress Analyses during High-Rate, Multiple Acid Jobs in Low-Permeability, HPHT Reservoirs, China
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Optimizations and Tubular Practice from Integrated Packer Stress Analyses during High-Rate, Multiple Acid Jobs in Low-Permeability, HPHT Reservoirs, China

机译:低渗透率HPHT油藏中高速率,多酸作业期间集成封隔器应力分析的优化和管实践

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This paper presents various case studies that were performed on an HPHT gas well located in the TarimrnBasin, China, with a primary focus on well completion, string design, and technique in response tornpacker-seal failure resulting from the interconnection of production casing pressure when conductingrnstaged acid jobs with a straddle-packer string. After tripping out, it was discovered that the upper packerrnmandrel was broken. This paper discusses the factors that led to the broken mandrel and packer-sealrnfailure and provides a unique solution to these challenges during staged acid jobs.rnBased on a detailed investigation conducted at the scene and further post-mortem studies using anrnadvanced wellbore temperature simulator that integrates with tubing and packer-stress analyses, it isrnbelieved that acid jobs using a heavy-duty pump under high pump pressures have resulted in a rapidrntemperature drop inside the wellbore, causing possible liquid contraction within the enclosed spacernbetween the straddle packers and, subsequently, decreasing the pressure. High differential pressurernbetween the upper and lower packer, as well as inside and outside of the enclosed space, can lead to arnbroken mandrel and packer-seal failure.rnThis paper discusses the failures that were analyzed using a comprehensive model that integrates withrntubing and packer-stress analyses by implementing multiple iterations and conditions with variations inrnpressure that were established between the packers during acid jobs. In addition, the string mechanicalanalysisrnmethod was used for the staged acid jobs. Based on case studies on the different methods forrnmitigating string challenges, a method was selected as the primary measure for improving string safetyrnduring staged acid jobs for high-pressure wells, which has been successfully applied in staged acid-jobrnoperations for two wells in this field.rnVarious models for tubing and packer mechanical analysis for staged acid jobs were established,rnproviding a better understanding of pressure with change in temperature within the enclosed spacernbetween packers. The results were able to explain the causes of packer failure from the string mechanicalrnpoint of view, which identifies the effect of various parameters on pressures within the enclosed space andrnthe effect of pressure change to the packer and tubing stresses. The results were supported by a detailedrninvestigation conducted at the wellsite.rnThe thesis of this paper introduces various methods for improving the safety of packers and strings,rnincluding increasing the temperature of injected fluid, tapping on the string between packers, andrnoptimizing string design. Based on analysis and field study, tapping on the string between packers hasrnbeen the best measure for improving string safety during staged acid jobs for high-pressure wells in thisrnfield.
机译:本文介绍了在中国塔里木盆地的一台HPHT气井上进行的各种案例研究,主要侧重于完井,管柱设计和技术,以应对在进行分段生产时由于生产套管压力相互连接而导致的封隔器-密封失效带有跨接封隔器字符串的酸作业。跳闸后,发现上部封隔器芯轴损坏。本文讨论了导致心轴破裂和封隔器-密封失效的因素,并为分阶段的酸工作提供了独特的解决方案。基于现场进行的详细调查以及使用先进的井眼温度模拟器(集成)进行的事后研究通过油管和封隔器应力分析,人们认为在高泵压下使用重型泵进行酸作业会导致井筒内部的温度快速下降,从而导致跨式封隔器之间的封闭式隔层内可能发生液体收缩,进而降低压力。上下封隔器之间以及封闭空间的内部和外部之间的高压差都可能导致缠结的心轴和封隔器-密封失效。本文讨论了使用集成了漏斗和封隔器-应力的综合模型分析的故障。通过在酸作业期间在封隔器之间建立具有不同压力的多次迭代和条件来进行分析。另外,串机械分析方法用于分阶段的酸作业。基于对缓解管柱挑战的不同方法的案例研究,选择了一种方法来提高高压井分段酸作业期间管柱安全性的主要措施,该方法已成功应用于该领域的两口井的分段酸作业中。建立了用于分段酸作业的各种油管和封隔器机械分析模型,以更好地理解封隔器之间封闭的垫片内温度随温度变化的压力。该结果能够从管柱机械角度解释封隔器失效的原因,其确定了各种参数对封闭空间内压力的影响以及压力变化对封隔器和管道应力的影响。本文的结果得到了在井场进行的详细研究的支持。本文介绍了多种提高封隔器和管柱安全性的方法,包括提高注入液温度,敲击封隔器之间的管柱以及优化管柱设计。根据分析和现场研究,敲击封隔器之间的管柱已成为提高该油田高压井分段酸作业期间管柱安全性的最佳措施。

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