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Case Study: Troubleshooting Centrifugal Compressor Trips Caused by HighVibration on Drive End Journal Bearing

机译:案例研究:通过驱动端期刊轴承高振动引起的离心压缩机跳闸故障排除

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Why can even the most reliable turbomachinery get tripped up? In some cases, it's all about bad vibrations--literally. This paper explores the challenges one site had with repeated centrifugal compressor trips causedby high vibration over a period of 25 days. It outlines the troubleshooting attempts made to remedy thisissue, it's root cause, and the resulting solution. This issue occurred at a site with a train configuration of gas turbine driven centrifugal compressors.After 48 hours of its first startup, the machine tripped due to high vibration at the compressor drive end.Initial attempts to fix the problem included checking the vibration probe gap voltage setting, as well asswapping vibrations probes. After these tasks were completed, the site again attempted to run the machine.48 hours later, it tripped again. During this time, the vibration gradually increased, staying above the alarmof 50 microns and tripping at 70 microns. The trip setting was increased to 75 microns, but after restarting,the unit continued to trip due to high vibrations. All components were removed and thoroughly examined. Clearances were measured per the standardchecklist. The condition of the couplings was found to be normal. The journal bearing pads had minorscratches. The thrust bearing pads were not affected by the failure. Alignment readings were found to benormal. However, residual unbalance was found on the rotor. This residual unbalance was found to be the root cause of the tripping issue. The journal bearingclearances were thus adjusted from 0.17 mm to 0.13 mm. It was also advised to perform high speed balancingchecks in the manufacturer's facility. The lube oil inlet pressure was adjusted to meet the requirements forthe new bearing clearance. Adjusting the bearing clearance, along with the adjustments in lube oil inlet pressure, resulted in improvedvibration readings. This case study provides the detailed analysis of the root cause of the frequent trips aswell as the process that was followed to fix the problem.
机译:为什么甚至可以绊倒最可靠的涡轮机会?在某些情况下,这完全是关于糟糕的振动 - 字面意思。本文探讨了一个站点的挑战,其中一个网站在25天内导致高振动的重复离心压缩机跳闸。它概述了对补救措施的故障排除尝试,它是根本原因和生成的解决方案。这个问题发生在一个火车涡轮机驱动离心压缩机的火车配置的网站。首次启动的48小时后,机器由于压缩机驱动器端的高振动而跳闸。尝试解决问题包括检查振动探测间隙的问题电压设置,以及振动振动探头。完成这些任务后,该网站再次尝试在后面运行机器.48小时后,它再次跳闸。在此期间,振动逐渐增加,保持在50微米的警报上方并在70微米下跳闸。跳闸设定增加到75微米,但重新启动后,由于高振动,该单位继续跳闸。除去所有组分并彻底检查。按照标准检查列表测量间隙。发现联轴器的状况正常。轴承垫的轴承垫具有迷人。推力轴承垫不受失败的影响。对对准读数被发现为百种数。然而,在转子上发现残留的不平衡。发现这种残差不平衡是跳闸问题的根本原因。因此,轴颈轴承率从0.17mm调节到0.13mm。它还建议在制造商的设施中进行高速平衡。调整润滑油入口压力以满足新的轴承间隙。调整轴承间隙,随着润滑油进油压的调整,导致改变振动读数。本案例研究提供了对频繁旅行的根本原因的详细分析,因为遵循解决问题的过程。

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