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Lessons learned from analyzing an explosion accident at Shanghai Secco chemical plant

机译:从上海塞科化工厂分析爆炸事故的经验教训

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On May 12, 2018, six workers from Shanghai Aijinke Engineering Construction Services Co., Ltd. died on the spot of an explosion when they were maintaining a benzene tank in the tank farm at Shanghai Secco Petrochemical Co., Ltd. The accident was characterized as a disastrous accident caused by hot work in a confined space, which resulted in massive casualties and a direct economic loss of 11.66 million yuan. This paper aims to analyze the accident occurrence process in a chronological order firstly by using the event sequence diagram (ESD). Multilayer Bow-tie Analysis was adopted to explore and classify the causes of the explosion of the benzene tank, along with the corresponding consequences, and the preventive measures. The analyses show that the primary inducements were the unsafe behavior of on-site workers, hazardous conditions of in-tank substances, risky factors in the construction environment, and deficiencies in management. Casualties, fire and explosion, equipment damage, and property losses were all included as consequences. The FLACS software was used to simulate the variation of explosion pressure and explosion temperature varying with time when benzene vapor was ignited at the tank bottom during the accident, and a flow field diagram for the explosion was achieved correspondingly. The results obtained are of direct significance for investigation of similar accidents in the future and are instructive to equipment safety evaluation as well. Based on the qualitative and quantitative analyses, we emphasize three considerable reasons leading to the accident, which includes inapposite flammable gases detection points before the hot work, failing to test the flammable gases during the hot work, and deficiency of the Management of Change (MOC). Finally, the paper concludes with a summary of lessons learned from the accident as well as suggestions for accident prevention and safety improvement.
机译:2018年5月12日,来自上海Aijinke工程建设服务有限公司的六名工人在上海塞科石化有限公司维持坦克农场的苯坦克时,在爆炸上死亡。事故表现了作为一个受限空间中的热门工作引起的灾难性事故,导致大规模伤亡,直接经济损失为1166万元。本文旨在首先通过使用事件序列图(ESD)以时间顺序分析事故发生过程。采用多层蝴蝶结分析来探索和分类苯罐爆炸的原因,以及相应的后果和预防措施。分析表明,主要诱导是现场工人,罐内物质危险条件,施工环境风险因素的不安全行为,以及管理缺陷。伤亡,火灾和爆炸,设备损坏以及财产损失都被称为后果。 FLACS软件用于模拟爆炸压力和爆炸温度随时间变化的变化,当时在事故过程中坦克底部点燃苯蒸气,相应地实现了爆炸的流场图。所获得的结果对于对未来的类似事故进行调查具有直接意义,对设备安全评估有影响。基于定性和定量分析,我们强调了导致事故的三种相当大的原因,其中包括在热处理前的Itapposite易燃气体检测点,未能在热工作期间测试易燃气体,以及变化管理的缺陷(MOC )。最后,本文总结了从事故中汲取的经验教训以及事故预防和安全改进的建议。

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