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Cost Effective Water Shut-Off: Slickline Conveyed High Expansion Ratio Through Tubing Bridge Plug

机译:经济高效的水关闭:Slickline通过管道桥插头传达高膨胀比

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In the recent low oil price environment,a cost-effective solution was proposed to use through tubing bridge plugs to perform water-shut-off(WSO)in an offshore field. The solution consisted of using slickline to set a plug with a high expansion ratio followed by a cement dump. After three WSO jobs in different wells,the method has successfully proven itself. Watercut was reduced from 100% to 0% with a minimal cost of only USD100,000. The through tubing bridge plug used is capable of passing through 2-7/8-in. tubing and expanding into 9-5/8-in. casing. After running a Gamma-Ray log,the plug was set across the perforation interval to give the anchor contact with a rough casing surface. The top of the plug,however,was above the perforation interval and became the base for cement. Cement was then continuously dumped on top using a slickline dump bailer in a static condition until the designed cement height was reached. Static conditions ensured no movement of cement during operation. The plug differential pressure limit is directly proportional to the cement height. The first WSO job was a complete success with watercut reduced from 100% to 0%. The second job however,was partially successful as the cement dump was not completed due to unexpected appearance of a hold-up-depth(HUD). The HUD was created by leftover cement which had accumulated at the end of the tubing. Despite the setbacks,the end result was successful in reducing water production from 1000 bwpd to 200 bwpd. The third job faced a completely different problem. The original plug fell off deeper into the well after it was set. To rectify the situation,a second plug was set at the target interval. Despite the successful execution,there was no change in watercut after the well was brought back online. Since the same method was proposed for another upcoming well,Memory-Production log(MPLT)coupled with Temperature-Noise log was performed to assess the effectiveness of the WSO. The log results confirmed that the WSO was successful and the post job water production was caused by channeling behind the casing. The results so far concluded that the through tubing bridge plug WSO method was both reliable and costeffective. It is exceptionally suitable for zones located at the bottom of a well and can be deployed using slickline. The paper provides valuable insight to a WSO solution which should be a first-choice option due to its relatively inexpensive cost and high reliability. The solution has proven to provide tremendous cost saving for production enhancement activity.
机译:在最近的低油价环境中,建议通过管道桥插头使用成本效益的解决方案,以在海上场中执行水关闭(WSO)。该解决方案包括使用Slickline设置具有高膨胀比的插头,然后是水泥倾卸。在不同井的WSO工作之后,该方法已成功证明自己。 Watercut从100%降至0%,最小成本仅为100,000美元。通过使用的通过管桥插头能够通过2-7 / 8英寸。管道和膨胀成9-5 / 8英寸。套管。运行伽马射线日志后,将插头横跨穿孔间隔设置,以使锚与粗壳表面的锚接触。然而,插头的顶部高于穿孔间隔,并成为水泥的基础。然后在静态条件下连续使用光滑倾卸桶将水泥倾倒在顶部,直到达到设计的水泥高度。静态条件确保在运行过程中没有水泥。插头差压限制与水泥高度成比例。第一个WSO工作是一个完整的成功,铁路从100%降至0%。然而,第二份工作是部分成功,因为由于持有升起深度(HUD)的意外外观未完成水泥倾倒。 HUD由剩余的水泥产生,该剩余水泥积聚在管道末端。尽管挫折,最终结果成功地将水产产量从1000 BWPD降至200 BWPD。第三个工作面临完全不同的问题。在设置后,原来的插头倒入了良好状态。为了纠正情况,将在目标间隔设置第二个插头。尽管执行了成功,但在井中恢复了网上后,卫星没有变化。由于对另一个即将到来的较好的方法提出了相同的方法,因此进行了与温度噪声日志耦合的内存制作日志(MPLT)以评估WSO的有效性。日志结果证实,WSO成功,后岗位水生产是由套管后面引起的。到目前为止,结果得出结论,通过管道桥塞WSO方法既可靠且成本有效。它非常适合位于井底的区域,可以使用Slickline部署。本文由于其相对廉价的成本和高可靠性,对WSO解决方案提供了有价值的洞察力。该解决方案已证明为生产增强活动提供了巨大的成本节约。

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