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Associated Polymer ASP Flooding Scheme Optimization Design and FieldTest after Polymer Flooding in Daqing Oilfield

机译:大庆油田聚合物洪水中的相关聚合物ASP洪水方案优化设计与现场税

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There are 54 blocks entered into subsequent water flooding period after polymer flooding in Daqing oilfield,The comprehensive water cut is as high as 97.2% and the average oil recovery factor is 57% for the reservoirafter polymer flooding,There are 44% geological reserves still remained underground and these reserves areof good quality for further exploitation.But the reservoir has gone through deepen development by tertiaryoil recovery and entered into the period of the fourth enhanced oil recovery,so how to further enhance oilrecovery is a world's toughest problem.Therefore a new oil displacing system with high efficiency shouldbe developed suitable for the reservoir after polymer flooding in order to greatly enhance oil recovery forultra-high water cut reservoir after polymer flooding.In this paper,lots of lab experiments have been carried out consisting of oil displacement performanceevaluation and formula optimizing.A new ASP formula using associated polymer has been developed,theincremental oil recovery of this system is 10.35% in the lab experiments of natural cores after polymerflooding.In contrast to linear polymer ASP system,associated polymer ASP system can reduce polymerdosage by 48% and increase oil recovery by 3.3% at the same time.The reservoir engineering and oildisplacement scenarios have been worked out and the field test has been carried out in the N3D block with 16injection wells and 25 production wells after polymer flooding in Daqing oilfield.The numerical simulationpredicts the incremental oil recovery can reach up to 8.76% after polymer flooding.The test has entered into field and obtained good technological and economic development effect.Theblank water flooding began in Sep 2012 and the trial injection of ASP flooding began in Oct 2013 andthe main ASP slug began in Jun 2014.Till Oct 2019,the accumulative injection pore volume was 0.9104PV with the injection pressure increased by 4.7 MPa,water absorption thickness ratio increased by 27.1%,the biggest water cut decline of single well was 6.4% and the staged incremental oil recovery was 7.89%.At present,the accumulative oil production increment is 0.647 million barrels and the economic benefit is 32.35 million dollars.The numerical simulation prediction shows that the final accumulative oil productionincrement is 0.657 million barrels and the final economic benefit is 32.87 million dollars.This new technology and field test can enhance oil recovery greatly for ultra-high water cut reservoirafter polymer flooding and obtain good technological and economic development effect,so it has a broadapplication prospect and can be applied extensively in ultra-high water cut blocks after polymer floodingin Daqing oilfield.
机译:在大庆油田的聚合物洪水后,有54个块进入随后的水淹期,综合水切口高达97.2%,水平溢油系数为57.%,储蓄聚合物洪水为57%,还有44%的地质储备仍然存在地下,这些储备是进一步开发的好品质。但水库已经通过泰国石油恢复来深化发展,并进入第四次增强的石油恢复期,因此如何进一步加强油脂劳动是一个世界上最艰难的问题。因此高效率的位移系统应开发适用于聚合物洪水后的储层,以大大提高石油回收五芦荟高水库,在聚合物洪水之后。在本文中,已经进行了大量的实验室实验,包括油位移性能和公式。优化。已经开发了使用相关聚合物的新型ASP公式,该系统的增量油回收率在聚合后天然核的实验室实验中的10.35%。与线性聚合物ASP系统的对比,相关的聚合物ASP系统可以将聚合物减少48%并同时将油回收增加3.3%。已经制定了水库工程和商品普查情景,在大庆油田的聚合物洪水中,在N3D块和25个生产井的N3D块中进行了现场测试。聚合物后,数值模拟预期可增量高达8.76%。洪水。该测试已进入现场,获得了良好的技术和经济发展效果。2012年9月开始的白金水洪水开始,2013年10月开始试用ASP洪水,主要的Asp Slug于2014年6月开始。2019年10月,累计注射孔体积为0.9104pv,注射压力增加4.7mPa,吸水厚度比增加27.1% e最大的水削减率单位井是6.4%,分期的增量油回收率为7.89%。目前,累计油生产增量为0.647万桶,经济效益为3235万美元。数值模拟预测显示最终累计油生产量为6.57亿桶,最终的经济效益是3287万美元。这项新技术和现场试验可以提高石油恢复,为超高水削减水库聚合物洪水充分提升,获得良好的技术和经济发展效果,所以它有一个广泛应用前景,可在聚合物泛拓后的超高水切块中广泛应用于大庆油田。

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