首页> 外文会议>SPE Nigeria Annual International Conference and Exhibition >Coiled Tubing Intervention for the Actuation of Reservoir Formation Isolation Valve in a High-Pressure Gas Well
【24h】

Coiled Tubing Intervention for the Actuation of Reservoir Formation Isolation Valve in a High-Pressure Gas Well

机译:用于在高压气体中储存器形成隔离阀的旋转管道干预

获取原文

摘要

Well – K1 is one of 6 gas wells drilled and completed in an over-pressured gas reservoirs in-line with SPDC aspirations to leverage on the opportunities presented by deep and over-pressured gas plays in a bid to develop hydrocarbon reserves to meet existing gas supply commitments and growing domestic demands(driven by power and manufacturing sectors).The well sand-face completions incorporated a Formation Isolation Valve(FIV)which provided a temporary isolation of the high reservoir pressure(circa 9,400psi)allowing the safe deployment of the upper completions in a lower density fluid,thus creating a 3,200psi underbalance without the well flowing.Post well construction and prior to hooking up the well for production,an evaluation was made on the best well intervention method to actuate the closed FIV open,especially because the hydraulic "trip-saver" option of opening the FIV was deactivated during well construction making the mechanical option the only means.After due considerations of the well configuration,high reservoir and surface pressures,high differential pressure across the FIV and possibility of mud solids settlement on the FIV shifting profile hindering access,Coiled tubing(CT)was selected to deploy the FIV shifting tool to mechanically open the FIV.After many months of careful planning and preparation,the intervention was carried out successfully and the well tested to planned rate.This paper discusses the detailed job design and planning towards deployment of coiled tubing in a deep over-pressured well.Also highlighted are the key challenges and experiences gained which can be referred to as a benchmark for CT deployment in HPHT environment in the Niger delta.
机译:Well-K1是钻孔的6个气体井之一,在整个过压的气体储层中与SPDC展示,以利用深度和过度压力的气体在出价中发挥的机会,以开发碳氢化合物储备以满足现有的气体供应承诺和日益增长的内部需求(由电力和制造业驱动)。井砂面完井融入了形成隔离阀(FIV),其提供了高储层压力(大约9,400psi)的临时隔离,允许安全部署较低密度流体中的上部完成,从而产生3,200psi的不平衡,没有流动良好的流量。井井建设和在挂钩生产中的生产中,对最佳井干预方法进行了评估,致力于致力于封闭的FIV开放,特别是由于在井结构期间液压“跳闸”选项在井结构期间停用,使机械选项唯一的手段。在适当考虑的情况下选择井结构,高储层和表面压力,穿过FIV的高分压力和泥浆固体沉降的可能性在FIV移位型材妨碍进入,卷绕管道(CT)展开了FIV移位工具,以机械地打开FIV.AFER许多几个月的仔细规划和准备,干预成功地进行了良好的测试率。本文讨论了详细的工作设计,并规划朝着深压力的井中部署线圈。突出显示是关键挑战获得的经验,可以称为尼日尔三角洲HPHT环境中CT部署的基准。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号