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A Successful High-Ratio Hole Opening Utilising a Dual Underreamer Saved Drilling Time in a Shale Gas Exploration Well

机译:利用双重底部爆发器的成功高比孔开口在页岩气勘探中节省了钻井时间

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Well M is a vertical shale gas exploration well in Indonesia.The presence of overpressured shale formation dictated the requirement to have a 16-in.intermediate casing string between the 20-in.and 13.375-in.casing to cover an approximately 350-to 1000-m measured depth(MD)interval.The mandatory logging operation in all hole sections required a 12.25-in.pilot hole to be predrilled,to enable the logging tool to get a good measurement quality,before it was enlarged to 17.5 in.for setting the 13.375-in.casing.Several hole opening challenges needed to be considered in this operation: 1)The hole opening tool should pass the 16-in.casing inside diameter(ID)restriction(14.936 in.); 2)the tool needed to be applicable for hole opening with an existing pilot hole(bi-center is not a feasible option); 3)the tool should be able to open the shoe track from 12.25 in.to 17.5 in.for 13.375-in.casing run assurance; and 4)the hole opening needs to be as efficient as possible to eliminate multiple runs.A dual hydraulically expandable underreamer was proposed to answer all those challenges.The configuration consists of two underreamers with different opening capability,which satisfies the high-ratio opening requirement.The lower reamer opened the hole from 12.25 in.to 14.75 in.,and the upper reamer further opened the hole from 14.75 in.to 17.5 in.Because running a tandem underreamer is not a common operation,a thorough vibration analysis must be performed to ensure the tool reams in a stable condition,not only to avoid downhole tool failure but also to produce a smooth borehole.Hydraulics optimization is also critical to ensure both underreamer cutter blocks are fully opened during the run.The tandem underreamer successfully opened the hole from 12.25 in.to 17.5 in.in one run to the section TD from 980 to 1623 m MD(a 643-m interval).At the surface,both underreamer cutter blocks were still in a good condition with 0-0-NO cutter dull and in gauge condition,which showed a good stability.This is also supported by the success of the 13.375-in.casing run to bottom without any issue,indicating a good and smooth borehole.The tandem underreamer method successfully achieved the high-ratio hole opening objective and saved drilling time by eliminating the unnecessary trip for having two separate underreaming runs.The underreamer tool mechanism and the criteria by which the dual underreamer configuration became the solution to the main challenges in this case study were documented.The study showed that the prejob engineering work(vibration modeling using dynamic finite element analysis and hydraulics modeling)was a critical part in the success of the operation.
机译:MOTER M是印度尼西亚的垂直页岩气探。过度抑制的页岩形成的存在决定了在20-IN.和13.375-IN.CASING之间有一个16英寸的壳体绳索的要求。覆盖大约350 - 1000-M测量深度(MD)间隔。所有孔部分中的强制记录操作需要倾向于12.25-In.Pilot孔,以使测井工具能够获得良好的测量质量,并在其扩大到17.5之前获得良好的测量质量。为了设置13.375-in.Casing.Capstal oppe孔打开挑战在该操作中需要考虑:1)孔开口工具应通过16-In.Casing内径(ID)限制(14.936英寸); 2)用现有的先导孔适用于孔开口所需的工具(双中心不是可行的选择); 3)工具应能够从12.25 in.to.to 17.5 in.13.375-in.casing保证; 4)4)孔口需要尽可能高效地消除多个运行。提出了双液体可扩展的底部射击器,以回答所有这些挑战。该构造包括两个具有不同开放能力的次次衰退器,满足高比率开口要求。下铰刀从12.25 in in ob on。到14.75英寸,上部铰刀进一步打开孔,从14.75 in.to 17.5。因为运行串联底线不是常用操作,必须进行彻底的振动分析为了确保工具处于稳定状态,不仅可以避免井下工具故障,还可以生产平滑的钻孔。液压系统优化也是至关重要的,以确保在运行过程中串联膨胀器完全打开。从12.25 in.to 17.5 in.In一个运行到TD部分,从980到1623 M MD(一个643-M间隔)。表面,底部刀具块仍处于良好状态条件含0-0-无切割器钝和仪表条件,表明稳定性良好。这也得到了13.375-in.Casing的成功而在没有任何问题的情况下运行到底部的支持,表明串联良好和光滑的钻孔。串联底部的方法通过消除两个单独的底射流的不必要的跳闸成功实现了高比率孔开口目标和节省的钻井时间。底部底部底部底部底部底部底部突发手的标准成为这种情况下的主要挑战的解决方案记录了研究。该研究表明,Prejob工程工作(使用动态有限元分析和液压建模的振动建模)是运行成功的关键部分。

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