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Successful UBD Application through the Full Operation Cycle of the Production Section on an Exploration Gas Well in Thailand: A Case History

机译:成功的UBD申请通过在泰国勘探天然气的生产部分的完整操作周期:一个案例历史

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Major challenges faced by today's industry in drilling fractured carbonate reservoirs are formation damage and potential drilling problems such as fluid loss and differential sticking.To drill such formations,underbalanced drilling(UBD)technology has been used as it can intentionally keep the bottomhole pressure(BHP)lower than the pore pressure(PP),which will eliminate the near-wellbore damage,and mitigate drilling problems like fluid losses.This technology was also used onshore in Thailand,mostly for development wells with low-pressure reservoirs.Well-A,located in the fractured carbonate Pha Nok Khao(PNK)formation of northeast Thailand is an exploration well with expected reservoir pressure around 6,000 psi(13 ppg in equivalent density),whose operator was determined to utilize UBD for the production section in order to minimize formation damage and maximize and test productivity.The higher reservoir pressure leads to higher operational risks for UBD.While drilling,single-phase water based mud(WBM)was used to keep proper drawdown for this section.In order to have safe and efficient tripping operations,tandem downhole deployment valves(DDV)were utilized to provide ultrareliable isolation of the wellbore for all the trips during drilling,logging and completion,which eliminated the need to snub or kill the well-any of which would lead to potential formation damage and safety issues.After completion,isochronal well testing was conducted using the same UBD package and later,in order to obtain more data to determine whether the operator could commercially develop the field.After that,a long-term well-test operation was conducted by continuously flaring the well at variable rates for 15 days using the same package.As the well was in an underbalanced condition through all the operation phases,no formation damage,fluid losses and NPT happened during the whole operation.The use of same UBD package from drilling till well testing for the full operation cycle also minimized costs and rig time.This paper details the UBD approaches used to minimize formation damage and evaluate reservoir productivity for the Well-A in the PNK formation of northeast Thailand.
机译:主要挑战在钻探裂缝碳酸盐岩油藏面对当今行业中形成损害和潜在的钻井问题,如体液丢失和差sticking.To钻这类结构欠平衡钻井(UBD)技术已经被使用,因为它可以有意保持井底压力(BHP )比孔隙压力(PP),这将消除近井眼损害降低和类似的流体losses.This技术减轻钻井问题在泰国也用于陆上,多为开发井与低压reservoirs.Well-A,位于所述裂缝碳酸盐帕诺克考(PNK)的形成东北的泰国是一个勘探井与大约6000磅(13分在相等的密度),其操作者被确定为利用UBD用于生产部,以最小化形成预期储层压力损伤和最大化和测试生产力。更高的储层压力导致对UBD.While钻孔,单相水b高操作风险ASED泥浆(WBM)来保持适当的缩编本section.In才能有安全,高效的运营跳闸,串联井下部署阀(DDV)被利用来为所有人提供井筒ultrareliable隔离期间,钻井,测井的车次和完成,这消除了需要冷落或压井-其中的任何一个将导致潜在的地层损害和安全issues.After完成后,等时试井使用相同UBD包进行,并且之后,在为了获得更多的数据,以确定无论是运营商可以商业开发field.After的是,长期的精心测试操作通过连续按浮动利率使用相同package.As通过所有的操作扩口以及15天以及在欠平衡条件下进行阶段,没有形成损伤,流体损失和NPT整个operation.The使用相同UBD包的过程中发生的从钻井直到试井完整操作循环也被最小化的COS TS和钻机time.This本文详细介绍了欠平衡钻井办法来降低地层破坏和在PNK形成泰国东北部的评估井-A储层产能。

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