首页> 外文会议>International Conference on Industrial, Mechanical, Electrical, and Chemical Engineering >Bontang LNG Plant Operational Strategy to Manage Ethane Refrigerant Inventory during Low NGL Extraction
【24h】

Bontang LNG Plant Operational Strategy to Manage Ethane Refrigerant Inventory during Low NGL Extraction

机译:Bontang LNG工厂在低NGL提取期间管理乙烷制冷剂库存的操作策略

获取原文

摘要

Badak LNG experience declining feed gas flowrate and shifting gas composition into lower NGL content. As consequence, times required for bullet replenishment has become approximately 50 times slower and potentially cause start up delay due to lack of refrigerant for make-up. In other hand, during very low ethane rundown from process train, significant amount boil off gas (BOG) generated along the pipelines which lead to excessive ethane loss to fuel gas and lower ethane liquid accumulated in storage bullet. As mitigation one bullet was reactivated to buffer sufficient amount of inventory and bullet operating pressure is raised to expedite replenishment time during very low NGL extraction.
机译:Badak LNG经验将饲料气体流量和将气体组合物转移到较低的NGL含量中。 因此,由于缺乏制冷剂的制冷剂,子弹补给所需的时间大约较慢,并且可能导致启动延迟。 另一方面,在从过程列车的非常低的乙烷损失期间,沿管道产生的大量沸腾气体(沼泽),导致过量的乙烷损失燃料气体和储存子弹中积累的下乙烷液体。 由于减轻了一个子弹被重新激活以缓冲量足够的库存和子弹操作压力在非常低的NgL萃取期间加快补充时间。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号