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First Successful Chemical Application Water Shut Off Job in DualCompleted Well Short Tubing and Oriented Perforations to Enhance WellProductivity in Burgan South Kuwait

机译:第一个成功的化学应用水在双核数短管和面向穿孔中关闭工作,以提高伯根南科威特的软产品

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Greater Burgan Field has been producing from more than 70 years and brings many challenges with thematuring field.During the last decade almost all the new wells drilled were completed as dual completions tosimultaneously produce from two different formations in Burgan.As the workover rig activity tremendouslyincreased with the increased number of new wells per year,it has been a constant endeavor to carry outmaximum well intervention jobs possibly by rig less operations to reduce rig related OPEX and wellproduction down time during rig work over.One of the biggest long term challenges was to carry out well interventions in dual completions shorttubing,which was used to be considered inaccessible due to presence of tubing long in the well bore.Inview of above,most of the intended well interventions in tubing short were normally used to be proclaimedas work over candidate thereby increasing load on limited work over rigs.First time in Burgan a dual completion well was carefully identified to carry out water shut off job bychemical application and adding perforation by oriented perforation gun in short tubing.The tubing shortwas producing from BGSU reservoir and became ceased to flow due to lateral water encroachment whichwas evident from the recent PNC log.The formation layer below BGSM was still having oil potential andwas intended to produce after shutting off the upper layer BGSU.The Tubing Long was producing fromdeeper reservoir BGSL around 1200 BLPD with 50% W/C.This paper elaborates the procedures adopted during the execution of the job and selection process of thechemical squeeze technology.The best suitable chemical technology was selected after carrying out a careful& detailed approach towards different vendors.The step by step detailed program was prepared to squeezethe chemical in to existing perforations,cleaning to the desired depth,testing the squeezed perforations andadding new perforations below with oriented perforations gun.The results were quite encouraging with sustainable oil gain of 1400 BOPD and the detailed cost/payback analysis indicated the payback period of only 1.5 days of production.This successful job has opened a new era in the history of Burgan field and many other water shut offjobs may be successfully carried out without the need of rig work over.This not only will reduce the work load on rig work overs and save rig cost significantly but will also allow to increase the well productivitywith a very short period of well down time.
机译:更大的Burgan领域一直在生产超过70年,并带来许多与实验领域的挑战。过去十年的钻取几乎所有新的井都完成了双重完井,从Burgan中的两种不同的地层生产.Asport arif and invendryincly indiquerce每年的新井数量增加,可能是一个不断的努力,可能是通过钻机更少的操作来减少钻机相关的OPEX和钻机工作中的井喷时间的运作。最大的长期挑战是携带的双重完井中的干预措施,习惯于在上述井中存在的管道的存在而被认为是无法进入的。在上述井中的情况下,管道短路中的大多数预期井干预通常用于被宣告普罗德斯队在候选人上工作,从而增加有限工作的负担在钻机上。伯根队在Burgan中的一点井是仔细的识别在短管中进行水关闭工作,并通过面向穿孔枪在短管中进行穿孔。由BGSU水库产生的管道短路,由于近期PNC原木中的横向水侵蚀而停止流动。下面的形成层BGSM仍然具有油势和武装,旨在在关闭上层BGSU之后生产。管道长度从DDEEPER储层BGSL产生大约1200个BLPD,50%w / c。本文详细阐述了在执行工作期间采用的程序Chemical挤压技术的过程。在对不同供应商进行谨慎和详细的方法后,选择了最佳合适的化学技术。步骤逐步详细的程序,准备将化学品挤压为现有的穿孔,清洁到所需深度,测试挤压的穿孔下面的新穿孔与面向穿孔枪。结果非常讨厌勇于可持续的石油增益1400 BOPD和详细的成本/回报分析表明,投资回收期仅为1.5天。此成功的工作在伯根田历史上开辟了新的时代,许多其他水关闭了offjobs可能会成功携带如果没有钻机的需要。这不仅会降低钻机的工作负荷,并拯救钻机成本显着,但也将允许在很短的时间内增加井生产率。

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