首页> 外文会议>SPE Kuwait Oil Gas Show and Conference >Focused Engineering Initiative Produces New 16-in Roller Cone TCI Design to Solve Carbonate Drilling Challenges in Northern Kuwait
【24h】

Focused Engineering Initiative Produces New 16-in Roller Cone TCI Design to Solve Carbonate Drilling Challenges in Northern Kuwait

机译:专注的工程倡议生产新的16英寸滚子锥TCI设计,以解决科威特北部的碳酸盐钻孔挑战

获取原文

摘要

Interbedded formations with vastly different compressive strengths and blind drilling are two distinct challenges the operator must solve constructing a 16" hole section in Northern Kuwait. These issues can lead to cutting structure damage to roller cone bits resulting in low performance and downhole tool failure. In addition the operator strives to achieve fast ROP by applying high weight-on-bit (WOB) through the hard Dammam to Mutriba carbonate sections which can also cause damage to the tungsten carbide insert (TCI) bit's cutting structure. To manage the challenges, the operator's drilling team working in conjunction with the bit supplier launched a performance improvement initiative. The carbonate application was analyzed using finite element analysis (FEA) based dynamic simulation program to fully understand how to stabilize the bit in different downhole conditions and improve hydraulic efficiency. Based on the computer analysis and field run data, a new stable bit was designed. The new bit includes a specialized cutting structure configuration, improved hydraulics and optimized insert carbide grades to mitigate impact damage. A patented double sealed bearing was also utilized to improve durability and seal reliability The new roller cone bit design was run with an optimized drilling plan setting a record rate of penetration (ROP) in its first test run. The new bit design has enabled the operator to drill a challenging carbonate section of 4775 ft from Shoe to total depth (TD) with a record penetration rates (ROP) of 65.8 ft/hr achieving 7.7 % increase in ROP over the best performance in the same field. The authors will discuss the application challenges, analysis and resulting performance improvement.
机译:具有巨大不同的抗压强度和盲钻的互粘面挑战是两个不同的挑战,操作员必须解决构建北科威特的16“孔部分。这些问题可能导致滚筒锥体损坏导致性能低,井下工具失效。在此外,操作者努力打造通过施加高重上钻压(WOB)通过硬达曼到Mutriba碳酸盐部分,以实现快速ROP其也因由该碳化钨插入件(TCI)位的切削结构。损坏要管理的挑战,操作员的钻井团队与该位供应商一起使用的展示性能提高序列。使用有限元分析(FEA)的动态仿真程序分析了碳酸酯应用,以完全了解如何在不同的井下条件下稳定该位并提高液压效率。基于在计算机分析和现场运行数据上,设计了一个新的稳定位。T他的新位包括专用切削结构配置,改进的液压和优化的碳化碳化物等级,以减轻冲击损伤。专利的双密封轴承还用于提高耐用性和密封可靠性,新的滚子锥形位设计采用优化的钻井计划在其第一次测试运行中进行记录渗透率(ROP)。新位设计使操作员能够从鞋子到总深度(TD)钻取4775英尺的挑战碳酸盐部分,以65.8英尺/小时的记录渗透率(ROP)在最佳性能下实现ROP增加7.7%相同的领域。作者将讨论应用程序挑战,分析和结果改进。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号