首页> 外文会议>Abu Dhabi International Petroleum Exhibition Conference >First Successful Chemical Application Water Shut Off Job in Dual Completed Well Short Tubing and Oriented Perforations to Enhance Well Productivity in Burgan South Kuwait
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First Successful Chemical Application Water Shut Off Job in Dual Completed Well Short Tubing and Oriented Perforations to Enhance Well Productivity in Burgan South Kuwait

机译:第一个成功的化学应用水在双重完成的短管和面向穿孔中关闭工作,以提高伯根南科威特的良好生产力

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Greater Burgan Field has been producing from more than 70 years and brings many challenges with the maturing field. During the last decade almost all the new wells drilled were completed as dual completions to simultaneously produce from two different formations in Burgan. As the workover rig activity tremendously increased with the increased number of new wells per year, it has been a constant endeavor to carry out maximum well intervention jobs possibly by rig less operations to reduce rig related OPEX and well production down time during rig work over. One of the biggest long term challenges was to carry out well interventions in dual completions short tubing, which was used to be considered inaccessible due to presence of tubing long in the well bore. In view of above, most of the intended well interventions in tubing short were normally used to be proclaimed as work over candidate thereby increasing load on limited work over rigs. First time in Burgan a dual completion well was carefully identified to carry out water shut off job by chemical application and adding perforation by oriented perforation gun in short tubing. The tubing short was producing from BGSU reservoir and became ceased to flow due to lateral water encroachment which was evident from the recent PNC log. The formation layer below BGSM was still having oil potential and was intended to produce after shutting off the upper layer BGSU. The Tubing Long was producing from deeper reservoir BGSL around 1200 BLPD with 50% W/C. This paper elaborates the procedures adopted during the execution of the job and selection process of the chemical squeeze technology. The best suitable chemical technology was selected after carrying out a careful & detailed approach towards different vendors. The step by step detailed program was prepared to squeeze the chemical in to existing perforations, cleaning to the desired depth, testing the squeezed perforations and adding new perforations below with oriented perforations gun. The results were quite encouraging with sustainable oil gain of 1400 BOPD and the detailed cost/pay back analysis indicated the payback period of only 1.5 days of production. This successful job has opened a new era in the history of Burgan field and many other water shut off jobs may be successfully carried out without the need of rig work over. This not only will reduce the work load on rig work overs and save rig cost significantly but will also allow to increase the well productivity with a very short period of well down time.
机译:更大的伯根根领域从70多年来生产出来,并带来了成熟领域的许多挑战。在过去的十年中,钻取的几乎所有新的井都被完成为双重完井,同时从Burgan中的两种不同地层产生。随着工作台钻机活动随着每年的新井数量增加而增加,它一直努力通过钻机更少的操作来减少钻机在钻机工作期间减少钻机相关的OPEX和井生产停机时间来实现最大的井干预工作。最大的长期挑战之一是在双重完成短管中进行良好的干预,这是由于在孔孔中由于管道的存在而被认为是无法进入的。鉴于上述情况,管道短路中的大多数预期井干预通常用于宣布为候选的工作,从而增加了有限工作的负荷。首次在Burgan中首次进行双重完井,经过精心识别,通过化学应用,在短时间内通过面向穿孔枪添加穿孔,并在短时间内进行穿孔。管道短从BGSU储层生产,并且由于最近的PNC原木而言,由于横向水侵蚀而停止流动。 BGSM下方的形成层仍然具有油势,并且在关闭上层BGSU之后产生。长度从深层储层BGSL生产,大约1200 BLPD,50%w / c。本文详细阐述了在执行化学挤压技术的工作和选择过程中采用的程序。在对不同供应商进行谨慎和详细的方法后,选择了最好的合适的化学技术。准备逐步详细的程序,以将化学物质挤入现有的穿孔,清洁到所需深度,测试挤压的穿孔并在下面用定向的穿孔枪添加新的穿孔。结果非常令人鼓舞,可持续投机1400 BOPD,详细成本/偿还分析表明,投资回收期仅为1.5天。这项成功的工作在伯根领域的历史上开辟了一个新的时代,并且许多其他水关闭就业人可以成功地进行,而无需钻机的需要。这不仅会降低钻机的工作负荷,并显着拯救钻机成本,但也将在很短的时间内延长良好的生产率。

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