首页> 外文会议>Abu Dhabi International Petroleum Exhibition Conference >Successful Installation of Tubing Patches to Restore Well Integrity Leads to Remarkable CAPEX Saving at Water Disposal Well WDW
【24h】

Successful Installation of Tubing Patches to Restore Well Integrity Leads to Remarkable CAPEX Saving at Water Disposal Well WDW

机译:成功地安装管材贴片以恢复井诚信导致卓越的资本资本资本资本支付良好

获取原文

摘要

The objective of writing this success story is to demonstrate how technology, in particular low cost solutions, are key to economically sustain and secure production from mature fields. Tubing Patch technology has been successfully utilized in Pakistan for the first time to restore the well integrity and saved huge CAPEX by avoiding expensive rig workover. Tubing-Annulus pressure suddenly increased in one of water disposal well (WDW). Annulus pressure varied directly with variations in Injection rates which were the clear evidence that tubing-annulus communication had been established and basic check ascertains that well had integrity issue. Being the only injector in area all production and processing of gas is majorly dependent on its injection reliability and integrity. After detailed in-house working it was decided to run diagnostic logging with spinner (quantitative) & temperature log (qualitative) to identify the leakage points precisely. All potential leakage paths (packer, tubing, tool joints) were considered while selecting the diagnostic techniques to have conclusive results. Based on diagnostic logging three leakage points were identified. Before proceeding for remedial measures to restore the well integrity, it was mandatory to check health of old carbon steel tubing string therefore it was planned to acquire corrosion log. Based on corrosion logging results, completion tubular was established in good condition which steered to install tubing patches best Techno-Economical solution across the leaks to restore well integrity instead of rig workover for re-completion. Consequently, three tubing patches, were successfully applied using wireline in water disposal well and integrity of well was restored. C-Annulus was pressure tested even after six months of installation and no pressure drop was observed during this interval.
机译:写作这一成功故事的目的是展示技术如何,特别是低成本解决方案,是经济上维持和从成熟领域生产生产的关键。第一次在巴基斯坦成功地利用了油管贴片技术,以恢复良好的诚信,并通过避免昂贵的钻机工作台挽救巨大的资本资本。管环压力突然在水处理井(WDW)中突然增加。环形压力直接变化,注射率的变化是明确的证据,即建立了油管 - 环通信和基本检查,即具有完整性问题。作为区域的唯一注射器,所有生产和加工的气体都主要取决于其注入可靠性和完整性。在详细的内部工作之后,决定使用旋转器(定量)和温度日志(定性)进行诊断日志记录,以确切地识别泄漏点。在选择诊断技术的同时考虑所有潜在的泄漏路径(包装机,管道,工具接头),同时选择具有确凿结果的诊断技术。基于诊断测井,识别出三个泄漏点。在继续进行补救措施以恢复良好的诚信之前,因此必须检查旧碳钢管道弦的健康,因此计划获得腐蚀日志。基于腐蚀测井结果,完成管状的良好状态,转向安装管道贴片最佳技术经济解决方案,泄漏以恢复良好的完整性而不是钻机工作组重新完成。因此,三个管材贴片,在水处理中成功应用了水处理,并且恢复了井的完整性。即使在安装六个月后,C-环空被测试,并且在该间隔期间没有观察到压降。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号