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Achieving 50 Plus Oil Production in Asphaltene-Stabilized Emulsion Problematic Field Under Artificial Lift Operation

机译:在人工升力操作下实现沥青质稳定乳液有问题场的50%加油

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An oil well in Japan, referred to in this paper as Well B, experienced emulsion problems from the commencement of natural flow production in January 2008. These problems were immediately resolved by the usage of effective demulsifier which was selected through bottle tests. As the well ceased to flow naturally in April 2014, an artificial lifting operation began with a jet pump since July 2014 to maintain the production rate. Shortly after artificial lifting performed, serious emulsion problems recurred even though it was continued to utilize the demulsifier which had worked successfully during natural flow. This paper presents the details of how we addressed these problems and managed to continue operations. Temperature, retention time and chemical injection were well known as the factors for separating emulsion. First, plant operator planned to raise the processing temperature from the current operating condition of 60°C. However, it was found that temperature higher than 60°C could damage coating inside gun- barrel and tanks which were located downstream of the second separator. Through fine optimization, the processing temperature was set at 65°C not to expose them to higher than 60°C but this was not feasible to separate emulsion. Second, we changed the flow scheme of two production separators from parallel to series connection. This countermeasure didn't resolve these problems essentially but it enabled us to catch almost all emulsions at the first separator. It means that the first separator condition could be reset by draining emulsion periodically from dump valve so that we managed to continue operations with keeping the target water content in sales oil. Finally, a series of bottle tests were conducted to select a better demulsifier to replace the original one, which was no longer effective. Soon after injection of the new demulsifier, the emulsions disappeared and the operator regained the production rate. This improvement reduced the emulsion disposal cost and man-hour for treating emulsions. Furthermore, oil which had been disposed as emulsions could be sold as product and Net Present Value (NPV) of this asset increased through high production rate operations. The total amount of economic impact reached 2 million dollars.
机译:油井在日本,本文以及B所指,从自然流动生产开始于2008年1月有经验的乳化问题,这些问题立刻被它是通过瓶试验选择有效的破乳剂的使用解决了。作为国内不复存在于2014年4月自然流动,人工吊装作业开始自2014年7月的喷射泵来维持生产速度。人工举升执行后不久,严重的乳化问题复发,即使它继续利用其天然了流动过程中成功合作的破乳剂。本文介绍了如何解决这些问题,并设法继续操作的细节。温度,停留时间和化学剂注入是众所周知的作为用于分离乳液的因素。首先,工厂操作员计划从60℃的当前操作条件提高加工温度。然而,已经发现,温度超过60℃会损坏gun-桶和分别位于所述第二分离器的下游油舱内涂层。通过精细优化,处理温度设定在65℃下不将它们暴露于高于60℃,但这不是分离的乳液是可行的。其次,我们改变了两个生产分离器中的流动方案从并行到串行连接。这种对策并没有本质上解决这些问题,但它使我们在第一分离器捕捉几乎所有的乳液。这意味着,第一分离条件可以通过从排水阀周期性排水乳液,使我们成功地继续保持在石油销售目标含水量操作复位。最后,一系列的瓶测试进行选择更好的破乳剂,以取代原来的一个,这已不再有效。新的破乳剂注射后不久,乳液消失,运营商恢复生产速度。这一改进降低了乳液的处置成本和工时用于治疗乳液。此外,已被布置为包油乳剂可以作为产物和该资产通过高生产率的操作增加的净现值(NPV)进行销售。经济影响的总额达到200万美元。

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