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Study and Application of Fuzzy Ball Micro Bubble Temporary Plugging Technology

机译:模糊球微泡临时堵塞技术的研究与应用

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Using cement to plug channeling as the conventional method is easy to pollute formation when the cement quality of oil well is bad or there is channeling between oil layer and water layer. In order to solve the problem of formation pollution fuzzy ball micro bubble temporary plugging technology is studied. Fuzzy ball micro bubble can't reverse rock wettability and can't stop fluids of reservoir flowing. The properties of rheology, static plugging and dynamic pollution were evaluated. The laboratory experiment proved that the fuzzy ball micro bubble has good inject ability and its viscosity decrease with shear rate. Under the temperature of 120 °C, back pressure of 0.5MPa and differential pressure of 5MPa, the leakage of fuzzy ball micro bubble was 0.Core permeability recovered ratio was up to 96.1% after pollution for 48 hours. The technology has been used on four wells in Jidong oilfield. The results of pilot test showed that the effect of decreasing produced water and increasing oil production was very obvious. The cumulative quantity of oil was 12435 t; the cumulative decreased quantity of water was 32496 cubic meters and the average water cut had decreased by 17.6%. The experimental evaluation and application effect indicates that the technology not only can reduce the operating risk but also has good plug channeling and layer protecting effect. After it is used on spot, the effect of increasing oil production and reducing aquifer yield is obvious and the period of validity is much longer.
机译:使用水泥堵塞窜作为常规方法是容易污染的形成时的油水泥质量好是坏的或有油层和水层之间窜。为了解决地层污染问题,研究了模糊球微泡临时堵塞技术。模糊球微泡不能反向岩石润湿性,不能停止水库流动。评估流变学,静电堵塞和动态污染的性质。实验室实验证明,模糊球微泡具有良好的注入能力,其粘度随剪切速率而降低。在120°C的温度下,背压为0.5MPa和5MPa的差压,模糊球微泡的泄漏是0.core渗透率恢复的比率在污染后达到96.1%,达到48小时。该技术已在冀东油田的四个井上使用。试验试验结果表明,降低产量和增加石油产量的效果非常明显。累积的油量为12435吨;累积的水量下降32496立方米,平均水切削率下降了17.6%。实验评估和应用效果表明该技术不仅可以降低运行风险,而且还具有良好的插头沟渠和层保护效果。在现场使用后,增加石油产量和减少含水层产量的效果是显而易见的,有效期更长。

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