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Paper Title Successful Optimization of Steam Flooding Pilot Test Project in Sudanese Oil Field Fula North East - Block 6

机译:苏丹油田富达东北汽水洪水试验项目纸质冠军冠军冠军

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Steam flooding is acontinues steam injection heats a large portion of the reservoir while reducing oil viscosity and achieves the most efficient heavy oil recovery. FNE oil field started production since 2009. In 2010 a pilot Cyclic Steam Stimulation (CSS) was implemented and showed double oil production incremental. Then full field Cyclic Steam Stimulation (CSS) was carried out, in September 2015 steam flooding pilot project was started with obvious increament. In this paper, an evaluation and optimization are made for the pilot test project in line with design, implementation, and production performance of the steam flooding pilot test in Fula North East. This paper will present the results from a study that done using advanced thermal software simulator on a sector model that extracted from FNE full field model, pilot area coverage 4 injectors and 9 producers. History matching and optimization was carried out along with perforation interval, steam intensity, steam quality and production rate. Optimum run case was determined among different sensitivity runs. The results show that oil production performance of steam flooding had significant effect on enhancing oil production. Oil rate increased from 715.66 to 1733.8 BOPD and clear water cut dwindled. After the optimization of steam injection parameters and perforation intervals observable increment in production was achieved, oil production rate increased from 966 to 1160 BOPD and clear water cut decreased.
机译:蒸汽洪水是蒸汽蒸汽喷射加热大部分储层,同时降低油粘度并实现最有效的重油回收。自2009年以来,FNE油田开始生产。在2010年,实施了试验循环蒸汽刺激(CSS)并显示出双油生产增量。然后进行全场循环蒸汽刺激(CSS),于2015年9月,蒸汽泛滥试点项目开始以明显的增量开始。在本文中,符合Fula North East蒸汽洪水试验试验的设计,实施和生产性能,对试点测试项目进行了评估和优化。本文将介绍一项研究的研究结果,这些研究在从FNE全场模型中提取的扇区模型上使用先进的热软件模拟器完成,导频区域覆盖4喷射器和9个生产商。历史匹配和优化以及穿孔间隔,蒸汽强度,蒸汽质量和生产率进行。在不同的灵敏度运行中确定了最佳运行情况。结果表明,蒸汽洪水的油生产性能对提高石油生产具有显着影响。油价从715.66增加到1733.8个博多和透明水被削弱。在蒸汽注射参数和穿孔间隔的优化之后实现了生产的可观察到,石油产量从966增加到1160普波德,透明水切口下降。

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