首页> 外文会议>Power Plant Pollutant Control MEGA Symposium >A DSI System Installation at a Midwest Utility: A Low-Cost Pollutant Control Solution
【24h】

A DSI System Installation at a Midwest Utility: A Low-Cost Pollutant Control Solution

机译:在中西部用力的DSI系统安装:低成本的污染物控制解决方案

获取原文

摘要

Dry sorbent injection (DSI) systems have been in service for more than 20 years at coal-fired generating stations, providing an effective tool for reducing sulfur dioxide acid gas emission levels. Current and pending environmental regulations have prompted a revival of interest in DSI as a low capital-cost, multi-pollutant control solution. This paper describes the installation of a new dry sorbent injection (DSI) system at a coal-fired generating station (hereafter referred to as 'the station') owned by a cooperative (hereafter referred to as 'the utility') located in the Midwestern U.S. It also presents a before-and-after comparison of emission results. The utility did preliminary testing and proof of concept, during which it tried both 'trona' - trisodium hydrogendicarbonate dihydrate (Na_3(CO_3)(HCO_3)·2H_2O) - and sodium bicarbonate (NaHCO_3 but abbreviated here as SBC). The results showed that SBC would easily meet the utility's objective of approximately 82 percent removal of total sulfur dioxide (SO_2), so it proceeded with designing and building a system that would inject SBC. This project warrants discussion because it demonstrates an economical solution for enabling certain coal-fired energy facilities to comply with recently enacted air-quality regulations and thus remain viable. Using SBC, the DSI system achieves SO_2 removal percentages that rival the performance of scrubbers. DSI thus provides a feasible alternative for units for which it would not prove cost-effective to invest in a wet or dry flue-gas desulfurization (FGD) system.
机译:干草注入(DSI)系统在燃煤发电站的20多年中已经在使用,提供了减少二氧化硫酸性气体排放水平的有效工具。目前和待定的环境法规促使DSI兴趣复兴作为低资本成本,多污染物控制解决方案。本文介绍了在燃煤发电站(以下称为'车站')所拥有的燃煤发电站(以下称为'该实用程序')的新的干草注射(DSI)系统的安装在中西部美国它还呈现出发射结果的前后。该实用程序进行了初步测试和概念证明,在此期间尝试了“rona” - 三钠碳酸氢盐二水合物(Na_3(Co_3)(HCO_3)·2H_2O) - 和碳酸氢钠(NaHCO_3,但在此作为SBC缩写)。结果表明,SBC将很容易地满足效用的目的大约82%的除去总二氧化硫(SO_2),因此它进行了设计和构建一个注入SBC的系统。该项目保证讨论,因为它展示了一种经济的解决方案,使某些燃煤能量设施能够遵守最近颁布的空气质量法规,因此保持可行。使用SBC,DSI系统实现SO_2去除百分比,竞争滑移的性能。因此,DSI提供了可行的替代方案,其单位不能证明投资于湿法或干燥烟道气脱硫(FGD)系统的成本效益。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号