首页> 外文会议>SPE/IADC Middle East Drilling Technology Conference >Pioneer Step in Securing Gas Well with Through Tubing Retrievable Bridge Plug Under Highly Complex Circumstance (1st Time in the Middle East)
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Pioneer Step in Securing Gas Well with Through Tubing Retrievable Bridge Plug Under Highly Complex Circumstance (1st Time in the Middle East)

机译:在高度复杂的环境下通过管道可检索的桥塞(中东第1次)通过管道可检索桥塞固定气井的先驱步进

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During a tubing depressurizing operation in a sour gas producer, the Sub-Surface Safety Valve dislodged from the nipple profile, broke and stuck inside the tubing hanger, restricting accessibility to the well. Multiple attempts to recover the stuck fish via slick line in combination with a permanent magnet resulted in recovering a few broken pieces and revealed a limited clearance of 1.85” through the fish. The well was killed and attempts to secure the well by installing through tubing inflatable bridge plugs using coil tubing were unsuccessful. It was then decided to exclude the coiled tubing operation for well integrity purposes due to limited clearance as the coil tubing had to pass through broken fish and could get stuck compromising the X-tree valves operation and it was decided to carry out work over operation to recover the broken fish. The cost for well work over was estimated at $ 3.0 MM. An innovative approach to secure this gas well riglessly using through Inflatable bridge plugs setting with electric line was introduced and the job was conducted successfully after completing all the risk assessments saving the significant costs associated with rig intervention. Two 1-11/16” through tubing inflatable retrievable bridge plugs (TTIRBP) were set with electric line passing thru the limited access hole of the broken fish. Plugs were set inside 4-1/2” and 3-1/2” tubing and pressure tested to 3000 PSI. The well was secured and the fish was successfully retrieved. Both bridge plugs were retrieved using 0.108 inches slickline and the well was put back into production. This great achievement was recognized as a 1st trial to carry out securing a sour gas well in the Middle East using a combination of electric line and slick line for setting and retrieving TTRPB Introduction Inflatable packers and plugs run on coiled tubing and wireline through production tubing for water & gas shut-off applications were introduced in late 1980s. This has brought substantial cost savings by eliminating the workover rig and all ancillary operations required by conventional workover in additional to bringing wells back to production in significantly less time. Expanding the use of thru-tubing retrievable beyond their usual scope, to secure wells where maintenance work was required on x-mas trees, tubing hangers and in this example to retrieve and replace the sub surface safety valve stuck in the tubing hanger in a rigless environment sheds light on a whole new range of applications. The rigless program designed and executed successfully to secure the sour gas well utilizing through tubing retrievable bridge plugs .
机译:在酸气体生产者中的管道减压操作期间,子表面安全阀从乳头型材脱落,破碎和卡在管道悬挂器内,限制了井的可接近性。多次尝试通过光滑线与永磁体相结合恢复卡氏鱼,导致恢复少量破碎的碎片,并通过鱼透露了1.85“的有限间隙。通过使用线圈管通过管道的充气桥插头安装,良好的良好并试图通过使用线圈管的充气桥插头进行良好。然后,它决定排除由于线圈管不得不通过破碎的鱼而导致的井完整性的线圈操作,因为线圈管必须穿过损坏的鱼,并且可以陷入困扰X树阀门的操作,并决定在操作上进行工作。恢复破碎的鱼。井的成本估计为3.0毫米。介绍了一种创新的方法,通过通过充气桥插头采用带电线的充气桥塞速度,并在完成所有风险评估后,在节省与钻机干预相关的大量成本的所有风险评估之后成功进行了作业。通过管道充气可回收的桥塞(TTIRBP)设定了两台1-11 / 16“,通过电线通过破碎的鱼的有限进入孔。插头内部设定在4-1 / 2“和3-1 / 2”管道内,压力测试到3000 psi。井被固定,鱼被成功检索。使用0.108英寸的光线和井回收桥接插头,井回到生产。这种巨大的成就被认定为第一个试验,以使用电线和光滑线的组合在中东地区进行酸性气体,用于设置和检索TTRPB引言充气封装机和塞管通过生产管道在盘绕的管道和有线线上运行在20世纪80年代后期推出了水和天然气关闭应用。这通过消除了常规管理器所需的所有辅助行动,在额外的情况下,这使得这使得大量节省了成本,以便在更短的时间内将井恢复到生产。扩大使用Thru-Tubing可重复于其通常范围,以确保在X-MAS树,管道吊架上需要维护工作的井,并在该示例中检索并更换胎盘悬挂器中的副表面安全阀在防盗器中粘在其中环境揭示了全新的应用范围。严格的程序成功设计和执行,以通过管道可检索的桥塞来固定酸气井。

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