首页> 外文会议>SPE/IADC Middle East Drilling Technology Conference >Pioneer Step in Securing Gas Well with Through Tubing Retrievable Bridge Plug Under Highly Complex Circumstance (1st Time in the Middle East)
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Pioneer Step in Securing Gas Well with Through Tubing Retrievable Bridge Plug Under Highly Complex Circumstance (1st Time in the Middle East)

机译:通过在高度复杂的环境下通过管道可检索桥塞(中东的第1次)通过管道可检索桥塞来保护气体

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During a tubing depressurizing operation in a sour gas producer, the Sub-Surface Safety Valve dislodged from the nipple profile, broke and stuck inside the tubing hanger, restricting accessibility to the well. Multiple attempts to recover the stuck fish via slick line in combination with a permanent magnet resulted in recovering a few broken pieces and revealed a limited clearance of 1.85” through the fish. The well was killed and attempts to secure the well by installing through tubing inflatable bridge plugs using coil tubing were unsuccessful. It was then decided to exclude the coiled tubing operation for well integrity purposes due to limited clearance as the coil tubing had to pass through broken fish and could get stuck compromising the X-tree valves operation and it was decided to carry out work over operation to recover the broken fish. The cost for well work over was estimated at $ 3.0 MM. An innovative approach to secure this gas well riglessly using through Inflatable bridge plugs setting with electric line was introduced and the job was conducted successfully after completing all the risk assessments saving the significant costs associated with rig intervention. Two 1-11/16” through tubing inflatable retrievable bridge plugs (TTIRBP) were set with electric line passing thru the limited access hole of the broken fish. Plugs were set inside 4-1/2” and 3-1/2” tubing and pressure tested to 3000 PSI. The well was secured and the fish was successfully retrieved. Both bridge plugs were retrieved using 0.108 inches slickline and the well was put back into production. This great achievement was recognized as a 1st trial to carry out securing a sour gas well in the Middle East using a combination of electric line and slick line for setting and retrieving TTRPB Introduction Inflatable packers and plugs run on coiled tubing and wireline through production tubing for water & gas shut-off applications were introduced in late 1980s. This has brought substantial cost savings by eliminating the workover rig and all ancillary operations required by conventional workover in additional to bringing wells back to production in significantly less time. Expanding the use of thru-tubing retrievable beyond their usual scope, to secure wells where maintenance work was required on x-mas trees, tubing hangers and in this example to retrieve and replace the sub surface safety valve stuck in the tubing hanger in a rigless environment sheds light on a whole new range of applications. The rigless program designed and executed successfully to secure the sour gas well utilizing through tubing retrievable bridge plugs .
机译:在中酸性气体生产的管道减压操作,分地面安全阀从乳头脱落轮廓,打破了和卡管悬挂器内,限制无障碍井。多次尝试用永磁恢复经由光滑线卡住鱼组合导致恢复一些碎片,并透露过鱼的1.85” 有限的间隙。该井被打死,企图通过管道使用连续油管充气桥塞是不成功的安装,以确保良好。当时决定为排除油井完整性的目的,连续油管作业由于有限的间隙为旋管必须经过破碎的鱼,可能会被卡住损害的X树阀门操作,并决定在运营工作进行到恢复碎鱼。井工作的成本比估计为$ 3.0mm以下。一个创新的方法,以确保该气井riglessly通过充气桥塞与电线引入和作业已完成所有风险评估节约与钻机干预相关的显著费用后成功地进行了设置使用。两个1-11 / 16” 通过管充气可回收桥塞(TTIRBP)分别设置有电气线路传递直通破碎鱼的有限访问孔。塞设置内部4-1 / 2” 和3-1 / 2” 管和压力测试,以3000 PSI。该井担保和鱼被顺利取出。这两个桥塞用0.108英寸钢丝检索和井恢复了生产。这个伟大的成就是公认的第一次审判,开展利用电力线和圆滑线的组合来设置和检索TTRPB介绍充气包装机在中东确保含硫气井和插头通过生产油管的连续油管和有线运行水和天然气关闭应用程序是在20世纪80年代末推出。这通过消除修井机和额外的常规修井需要把所有的井配套业务带来了可观的成本节约回生产显著更短的时间。扩大使用通油管回收超出自己平时的范围,其中被要求在采油树的维护工作安全的井,管道悬挂在这个例子中检索并替换子表面安全阀卡在管路悬挂在rigless环境阐明了应用的全新系列。设计并成功执行的rigless程序,以确保通过油管回收桥塞的含硫气井利用。

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