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Analysis of reservoir choke and broken down of Tong Liao uranium production

机译:塘辽铀生产水库扼流圈分析及分解

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This project aims at the phenomenon of increasing injection pressure of injection wells of the Tong Liao Uranium SW-8E test wells group, carries out the research of reservoir choke and broken down. By analysis of the water quality of injected and produced fluid through the test wells, scaling prediction, physical simulation experiments and other research, we find the main cause of clogging injection wells: Bacteria blockage, scale blockage, solids blockage and reservoir clay swelling blockage. Meanwhile according to the main reasons of reservoir pollution we have carried on pointed research of broken down, excogitate a better integrated and targeted reservoir choke Blocking Remover. Through on-site implementation, the injection pressure is reduced by 0.3-0.4MPa (maximum allowable injection pressure is 2.0MPa), well purge period is extended from three days to three months, this project solves the problems and achieves very good results.
机译:该项目旨在增加桐辽铀SW-8E试验井的注射孔注射压力的现象,进行水库扼流圈的研究并分解。通过通过测试井进行注射和产生的流体的水质,缩放预测,物理仿真实验和其他研究,我们发现堵塞注射孔的主要原因:细菌阻塞,尺度阻塞,固体堵塞和水库粘土膨胀阻断。同时根据水库污染的主要原因,我们在分解的尖锐研究中进行了探讨,摘要更好的集成和有针对性的水库扼流圈阻塞去除剂。通过现场实施,注射压力降低0.3-0.4MPa(最大允许注射压力为2.0MPa),井中净化时期从三天到三个月延伸,解决问题并实现了非常好的结果。

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