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Nondestructive testing for support quality of tunnel

机译:隧道支持质量的无损检测

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A tunnel in Chengde collapsed several times and cracks existed in the second lining. Using non-destructive testing equipment, tunnel support was detected to find out the hidden trouble early. In the section of K16+890~K16+950, the quality of tunnel support was assessed, with GPR and anchor measuring apparatus. In the tunnel, the thickness of composite lining was 25cm, and the second lining was 38cm, both of which met the design requirements. Positive peak method was selected to locate on I beam. The average longitude space of I beam was 127cm, while the design value is 120cm. Many rock bolts was lacked at the right crown. Moreover, the bolts in the haunch did not kept in diamond layout, close to I beam. Through analyzing waveforms of impact-echo, the number of qualified bolts only made up 74 per cent of the total bolts. The large space of I beam led to the lack of holding power. Meanwhile, the disqualified bolts limit the coordination deformation between surrounding rock and support. All the support defects led to tunnel collapse. These tests results demonstrate that NDTcan be used to mitigate the risks of tunnel construction.
机译:成都的隧道坍塌了几次,第二次衬里存在裂缝。使用非破坏性测试设备,检测到隧道支持,以便早期找出隐藏的麻烦。在K16 + 890〜K16 + 950的截面中,评估隧道载体的质量,具有GPR和锚定测量装置。在隧道中,复合衬里的厚度为25厘米,第二个衬里为38cm,两者都符合设计要求。选择正峰法以定位在I光束上。 I光束的平均经度空间为127厘米,而设计值为120厘米。右冠冕缺少许多岩石螺栓。此外,竖枢中的螺栓没有保持在金刚石布局中,靠近I梁。通过分析冲击回波的波形,合格螺栓的数量仅占总螺栓的74%。我梁的大空间导致缺乏持有权力。同时,取消资格的螺栓限制了周围岩石和支持之间的协调变形。所有支持缺陷导致隧道崩溃。这些测试结果表明,NDTCAN用于减轻隧道施工的风险。

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