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Practices Implemented to Achieve Record Performance in Narrow-Margin Drilling in Bass Strait Extended Reach

机译:实施实践,以实现低音海峡狭窄钻井钻井钻探的记录性能

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This paper discusses the successful application of the operator's drilling performance management process in the Australia Snapper / Moonfish platform drilling program. Snapper performance has historically been limited by shale instability, collapsing coal seams, lost returns, and other narrow margin drilling challenges. The design and execution practices implemented achieved record performance while simultaneously addressing the borehole behaviors that prevented the previous extended reach drilling (ERD) campaign from fully developing significant Moonfish resources. The operator's performance management process ensures both bit and non-bit limiters, such as borehole instability, are addressed with equal rigor, technology, and workflow. Issues that were previously viewed as trouble costs are treated as drilling performance limiters so solutions are pursued that both eliminate the trouble time and increase footage per day. The performance and borehole management practices implemented by the multifunctional team included: - Wellbore profile optimization to maximize shale and coal stability; - Specialized rig equipment and operational practices for equivalent circulating density (ECD) management; - Unique coal drilling practices to improve borehole stability; - Application of specialized hole cleaning equipment and surveillance; - Bit and bottomhole assembly (BHA) design to manage borehole quality while maximizing rate of penetration (ROP) and tool life; - Contingency planning for execution flexibility to respond to borehole limiters; - Office and field team training and alignment for flawless execution. The Moonfish M33a and Moonfish A26a extended reach wells were drilled to total depths of 20,341 and 21,180 ft, respectively. Both wells were completed under budget and are among the highest oil producers in the Bass Strait. The performance management process ensured that the borehole behaviors which had lowered the results of previous wells were addressed, while simultaneously achieving record setting performance. Interests in the Snapper and Moonfish fields are held by Esso Australia and BHP Billiton in a 50:50 joint venture
机译:本文讨论了运营商在澳大利亚Snapper / Moorfish平台钻井计划中的钻井性能管理过程的成功应用。 Snapper性能历来受到页岩不稳定性,坍塌煤层,损失返回和其他狭窄保证金攻击挑战的限制。实施的设计和执行实践实现了记录性能,同时解决了阻止前一个扩展钻井(ERD)运动的钻孔行为完全开发出显着的月尘资源。操作员的性能管理过程确保两个位和非比特限制器(例如钻孔不稳定性)以相同的严格,技术和工作流程解决。以前被视为麻烦成本的问题被视为钻井性能限制器,因此解决了解决方案,两者都消除了每天的故障时间和增加镜头。多功能团队实施的性能和钻孔管理实践包括: - 井眼轮廓优化,以最大化页岩和煤炭稳定性; - 用于等效循环密度(ECD)管理的专业钻机设备和操作实践; - 独特的煤钻练习,以提高钻孔稳定性; - 专业孔清洁设备和监测的应用; - 位和底孔组件(BHA)设计以管理钻孔质量,同时最大化渗透率(ROP)和刀具寿命; - 执行灵活性以响应钻孔限制器的应急计划; - 办公室和现场团队培训和结束执行的一致性。月状M33A和Moonfish A26A延伸井分别钻到20,341和21,180英尺的总深度。两个井都在预算下完成,并在低音海峡中的最高石油生产商之一。绩效管理过程确保了降低了先前井的结果的钻孔行为,同时实现了记录设置性能。塞诺澳大利亚和BHP Billiton在50:50的合资企业中举行鲷鱼和月球场的兴趣

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