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Productivity Improvements at Direct Chill Casting unit in Aluminium Bahrain (ALBA)

机译:铝合金巴林(Alba)直接冷藏铸造装置的生产力改进

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ALBA has been producing Rolling Ingots utilizing two DC casting units viz., DC1 & DC6. Out of total annual production of 140,000 MT of Rolling Ingot, DC6 production was 100,000 MT (1xxx, 3xxx & 8xxx series alloys) while DC1 production was 40,000 MT of 5xxx series alloy. Due to higher cost of production & low productivity at DC1, ALBA management decided to close down DC1 as a part of restructuring exercise and maximizing production at DC6 to meet customers demand. An extensive study was carried out towards improving productivity. Four levers of improvement which has the maximum impact were identified e.g., furnace preparation practices, preparatory activities between casts, increasing casting speed etc. Various action plans were drawn up & were implemented. These actions were closely monitored by DC operators themselves by using trend charts. As a result a 30% improvement in productivity was achieved at DC6 on a consistent basis.
机译:Alba一直在生产利用两个直流铸造单位viz的轧制锭。,DC1和DC6。在年产140,000公吨的轧制锭中,DC6生产是100,000吨(1xxx,3xxx和8xxx系列合金),而DC1生产是40,000吨5xxx系列合金。由于DC1的生产率更高,DC1的生产率低,Alba管理层决定关闭DC1作为重组运动的一部分,并在DC6最大化生产以满足客户需求。进行了广泛的研究,以提高生产力。确定了具有最大冲击的改善杆的杠杆,例如,熔炉准备实践,铸造之间的培训活动,增加铸造速度等。制定了各种行动计划并实施。通过使用趋势图表,DC运营商本身密切监测这些行动。结果,在DC6的基础上,在DC6实现了30%的生产率提高。

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