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Combating Severe Losses and Improving Cementing Quality in Carbonate Formations:A Lesson Learned from Drilling Wells in Offshore Sarawak, Malaysia

机译:在碳酸盐母组织中打击严重损失和改善固井质量:马来西亚海滨沙捞越钻井井中吸取的课程

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Wells drilled into gas bearing carbonate reservoirs in offshore Sarawak are prone to severe lost circulation issues.In the first 3 exploration wells,total losses were encountered after drilling 20 m into the carbonate in 8.5-in.hole section.The well managed to drill to TD with application of pressurized mud-cap drilling. However the challenge of the total losses wellbore is the incomplete cementing of the 7-in.liner across the carbonate column.Poor zonal isolation and reduction of reservoir permeability were major concerns to the operator requiring significant investigation,laboratory testing and pre-job planning for future wells. This paper will discuss operational,engineering,and unique design techniques for curing the chal-lenging lost circulation issues while also providing improved cement placement along the fractured formation.Lab test results are presented using a bridging material simulator with different fracture sizes to evaluate the sealing effectiveness of the engineered systems.Return permeability studies using a Hasseler-style core holder were conducted for the fluids to verify their damage potential to the producing formations. The engineered solution was the use of a cement spacer fluid containing membrane forming colloids to seal fracture sizes up to 2 mm which also yielded 100%return permeability to hydrocarbons.The use of the spacer fluid enabled successful cement placement along the critical carbonate section without any losses during cementing.A bond log evaluation showed that there was cement coverage along the zones of interest concluding the well had effective zonal isolation.Based on the positive lab tests and field results,the combination of a sealing spacer and lightweight cementing system was identified as a viable solution to combat lost circulation and improve cement placement for future wells drilled in this area.
机译:钻入在近海沙捞越气体轴承碳酸盐储层井容易发生严重漏失issues.In第一3口勘探井,总损失钻20米进入碳酸盐之后遇到在8.5 in.hole section.The管理良好的钻取到TD与加压泥浆帽钻孔的应用。然而井筒未完成固井跨越碳酸盐column.Poor区域隔离,降低储层渗透率的7 in.liner的总损失的挑战是,以运营商主要关注的问题,需要进行调查显著,实验室测试和预规划工作未来井。本文将讨论操作,工程和独特的设计技术用于固化CHAL-有挑战性漏失的问题,同时还使用桥接材料模拟器具有不同尺寸的断裂来评估密封提供改进的水泥放置沿裂隙formation.Lab试验结果呈现使用Hasseler式岩心夹持器的改造systems.Return渗透性研究的有效性进行了用于流体进行来验证其损害潜力的生产地层。该工程化的解决办法是使用含有膜形成性胶体以密封断裂水泥隔离液的尺寸可达2毫米,其也产生100%的回报渗透性hydrocarbons.The使用隔离液的使能沿临界碳酸酯部分成功的水泥放置而没有任何cementing.A胶结测井评价过程中的损耗结果显示,有沿的利益缔结了良好有效的纬向isolation.Based的积极实验室测试和现场试验结果区域水泥覆盖,密封垫片和轻质固井系统的组合被确定为一个可行的解决方案,以打击堵漏,提高在该领域未来的钻探油井水泥贴片。

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