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Entry, Descent, and Landing Performanceof the Mars Phoenix Lander

机译:火星凤凰兰德的入境,下降和着陆表现

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On May 25, 2008, the Mars Phoenix Lander successfully landed on the northern arctic plains of Mars. An overview of a preliminary reconstruction analysis performed on each en-try, descent, and landing phase to assess the performance of Phoenix as it descended is pre-sented and a comparison to pre-entry predictions is provided. The landing occurred 21 km further downrange than the predicted landing location. Analysis of the flight data revealed that the primary cause of Phoenix's downrange landing was a higher trim total angle of at-tack during the hypersonic phase of the entry, which resulted in Phoenix flying a slightly lift-ing trajectory. The cause of this higher trim attitude is not known at this time. Parachute deployment was 6.4 s later than prediction. This later deployment time was within the varia-tions expected and is consistent with a slightly lifting trajectory. The parachute deployment and inflation process occurred as expected with no anomalies identified. The subsequent parachute descent and powered terminal landing also behaved as expected. A preliminary reconstruction of the landing day atmospheric density profile was found to be lower than the best apriori prediction, ranging from a few percent less to a maximum of 8%. A comparison of the flight reconstructed trajectory parameters shows that the actual Phoenix entry, de-scent, and landing was close to pre-entry predictions. This reconstruction investigation is currently ongoing and the results to date are in the process of being refined.
机译:2008年5月25日,火星凤凰兰德成功登陆了火星北极平原。对每个EN-TRY,下降和降落阶段进行初步重建分析的概述,以评估Phoenix的性能,因为它被预先发出,并提供与进入前预测的比较。着陆发生了21公里,进一步下降了预测的着陆位置。对飞行数据的分析表明,凤凰的下游着陆的主要原因是在进入的高超声音阶段期间的近距离的较高的整体角度,导致凤凰飞行略微升力的轨迹。此时未知这种较高的修剪态度的原因。降落伞部署比预测晚6.4秒。此后部署时间在varia-tions预期,并且与略微提升轨迹一致。降落伞部署和通货膨胀过程发生在预期的情况下,没有发现异常。随后的降落伞血管下降和动力终端降落也表现得如预期。发现着陆日大气密度剖面的初步重建低于最佳的APRIORI预测,从少百分比达到最多8%。飞行重建轨迹参数的比较表明,实际的凤凰进入,失败和着陆是接近进入前预测。该重建调查目前正在进行,迄今为止的结果正在进行中。

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