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A Novel Foamer for Deliquification of Condensate-Loaded Wells

机译:一种新型发泡剂,用于淹没冷凝物加载的孔

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Continuous increase in worldwide brown-field activity and overall depletion of current gas fields has renewed focus on maximizing gas production from existing wells. In most gas wells, water and/or condensate is produced along with gas. In mature gas wells, decreasing formation pressures and gas velocities gradually cause the wells to become “loaded” with liquids. A method commonly used to deliquify these wells is through the application of chemical “foamers”. However, these traditional foamers tend to be ineffective as the condensate-to-water ratio increases. This paper describes the performance of a novel foamer specifically designed to unload condensate from wells. This foamer helped unload a gas well that produced condensate via intermittent production at 2:1 condensate-to-water ratio. Parameters for well selection are described, as well as operational processes to maximize continous production. As a result of this treatment, the daily average gas production rate increased significantly and shifted the daily on:off production cycle from 1:1 to 11:1. This minimized well down time and increased the overall daily production averages by 60 percent.
机译:全球棕色场活动的持续增加和目前气田的总体消耗已经重新设计了最大限度地利用现有井的天然气生产。在大多数气井中,水和/或冷凝物与气体一起生产。在成熟的气井中,逐渐降低形成压力和气体速度使井成为液体的“装载”。通常用于淹没这些孔的方法是通过应用化学“发泡剂”。然而,随着冷凝水与水比的增加,这些传统的发泡剂往往是无效的。本文介绍了专门设计用于从井中卸载冷凝物的新型发泡剂的性能。该发泡器有助于卸下通过在2:1冷凝物与水比中间歇生产产生冷凝物的气体。描述了井选择的参数,以及可操作过程以最大化连续生产。由于这种治疗,每日平均气体生产率显着增加,每日转移:从1:1至11:1中脱离生产周期。这最小化了更快的时间,并使整个日常生产平均值增加了60%。

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