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Water Management Challenge Turned into a Friendly EnvironmentalResponse Resulting from Successful Stimulations with Coiled Tubing inWater Injection Wells: Chichimene Field Case Study in Colombia

机译:水管理挑战变成了一种友好的环保响应,从而成功刺激卷绕管道水墨注射井:哥伦比亚的Chichimene田间案例研究

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Two producer wells in the Chichimene field of Colombia were converted to injector wells as part of a watermanagement and pressure control strategy.Because of zero injectivity in these wells,the operator desiredto stimulate for a successful disposal-type reinjection to decrease the 70,000 bbl of water being discharged.This paper describes the planning and performance of stimulation operations in these two injector wells.Aproper diagnostic helped to identify damage to be attributed to fines migration.Based on a consideration ofpetrophysical properties and corresponding logs,an acid system was designed and tested in the laboratory.Diversion options during stages of sequenced acid preflush,hydrofluoric acid,and postflush were reviewed.The desire to minimize the tubular exposure to acid in the wellbore and to place the open end of the tubingin front of the perforations made the option of coiled tubing appealing.With this option,the placement ofthe necessary sequential stages of the sandstone acid treatment would be possible across discrete intervals.Both wells experienced an injectivity index of zero before the acid treatment.The average daily injectionof well CH-182 dramatically increased to 19,000 BWPD after the acid treatment.The average daily injectionof well CH-183 dramatically increased to 20,000 BWPD after the acid treatment.These two wells currently have higher injection capacities than any other wells in the Chichimene field;combined,they inject 43,000 BWPD at maximum peak.The discharged water volume before the stimulationtreatments was 70,000 bbl.After stimulation of the injector wells,the discharged volume is 30,000 bbl,representing an approximately 60% reduction in discharged volume.
机译:在哥伦比亚的Chichimene领域中的两种生产井被转换为喷射器井,作为水管理和压力控制策略的一部分。由于这些井中的零喷射性,操作员希望刺激成功的处置型重新注射以减少70,000桶水本文介绍了这两个喷射器井中刺激操作的规划和性能.Aproper诊断有助于识别归因于罚款迁移的损伤。基于Persophysical属性和相应的日志,设计和测试了一种酸系统综述了测量酸素,氢氟酸和后灌水阶段的阶段的实验室选择。希望最小化井筒中酸的管状暴露,并将管子的开口置于穿孔的前部取代式管道吸引力。在此选项中,安置桑斯顿的必要顺序阶段酸治疗在离散间隔中是可能的。井在酸治疗前经历了零的重点指数。酸治疗后井CH-182的平均每日注射剧烈增加到19,000 bwpd。井CH-183的平均每日注射酸治疗后增加到20,000 bwpd。目前的喷射能力比下骨磁场中的任何其他孔更高;合并,它们以最大峰值注射43,000个BWPD。刺激溶剂前的排出水体积为70,000 bbl。喷射器孔,放电体积为30,000bbl,表示排出量的约60%。

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