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Pre-Job Modeling/Resulting Integrated BHA System Solution Sets Multiple ROP Records, North Field Qatar

机译:求职者预造型/由此产生的集成BHA系统解决方案设置多个ROP记录,北野卡塔尔

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Drilling the 12?-in tangent section (55-60°) through thick carbonate lithology in Qatar抯 offshore North Field is exceptionally challenging. In spite of bottom hole assembly (BHA) and parameter adjustments, the operator regularly experiences severe impact induced PDC cutter damage resulting in reduced bit life. Lithology (Hith to Khail) is predominantly interbedded carbonate/anhydrite, dolomite/argillaceous limestone with unconfined compressive strength (UCS) ranging between 9000-30,000psi. The operator wanted to improve rate of penetration (ROP) by stabilizing the bit body and reducing micro-balling tendencies. The objective would be to complete the 6000ft section in one bit run at a minimum ROP of 2000ft/24hr. An FEA-based modeling system, rock strength identification program and computational fluid dynamics (CFD) analysis was used to investigate several 12?-in PDC bit designs. The results of the simulations led to a new MSi716 design with back-up cutters strategically positioned on all blades to provide maximum durability in critical wear areas. After reviewing the results of the analysis, the operator requested additional bit design changes including a 6-in tapered gauge and managed depth-of-cut in the cone/nose areas to reduce reactive torque. A parameter sensitivity study was conducted to determine the optimal operating window (WOB/RPM) and to ensure the new PDC design would be compatible with a unique high-torque RSS which allows for higher weight on bit than standard rotary steerable systems to maximize rate of penetration potential. The new design was run on the high-torque RSS/motor system and drilled 6,001ft of 12?-in section at a high ROP of 139.4ft/hr setting a new North Field record. The average daily footage was 2572ft besting the old mark by 38%. Additionally, the run set a single 24hr footage record of 3100ft/day, 29% better than benchmark. Based on this outstanding bit performance the operator made these design changes a standard requirement for PDC bits in this application. The new design also helped standardize mechanical specific energy (MSE) values for future ROP gains.
机译:通过厚碳酸盐岩石钻钻12? - in切线部分(55-60°)在卡塔尔抯海上北场的厚碳酸盐岩石是特别挑战。尽管底部孔组件(BHA)和参数调整,但操作员经常经常经历严重的冲击诱导的PDC刀具损坏,从而降低了比特寿命。岩性(河洞到Khail)主要是碳酸盐/空矾石,白云石/骨质石灰石,具有不包含的压缩强度(UCS)在9000-30 000psi之间。操作员希望通过稳定钻头体并减少微球倾向来提高穿透速度(ROP)。目标是在2000英尺/ 24小时的最小ROP中完成6000英尺的部分。基于FEA的建模系统,岩石强度识别程序和计算流体动力学(CFD)分析用于研究几个12?-IN PDC位设计。模拟结果导致了一个新的MSI716设计,带有备份切割器,策略性地定位在所有刀片上,以在关键磨损区域提供最大的耐用性。在审查分析结果后,操作员请求额外的位设计变更,包括6英寸锥形仪表,并在锥形/鼻子区域中管理深度,以减少反应性扭矩。进行参数灵敏度研究以确定最佳操作窗口(WOB / RPM),并确保新的PDC设计与独特的高扭矩RSS兼容,允许比标准旋转可操纵系统更高的重量,以最大化速率渗透潜力。新设计在高扭矩RSS /电机系统上运行,并在139.4英尺/小时的高级ROP上钻了6,001英尺的12? - 截面,设置了新的北野记录。平均每日镜头为2572英尺,旧标记达38%。此外,运行设置了3100英尺/天的单个24小时录像记录,比基准更好。基于此出色的位性能,操作员使这些设计更改了本申请中PDC位的标准要求。新设计还有助于规范机械特定能源(MSE)值以供未来的ROP收益。

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