首页> 外文会议>SPE Annual Technical Conference and Exhibition >Standalone Sand Control Failure: Review of Slotted Liner,Wire Wrap Screen,and Premium Mesh Screen Failure Mechanism
【24h】

Standalone Sand Control Failure: Review of Slotted Liner,Wire Wrap Screen,and Premium Mesh Screen Failure Mechanism

机译:独立砂控制失败:速度衬里衬里,电线包装屏和高级网屏故障机制

获取原文

摘要

Standalone screen has been widely used as sand control solution in oil industries for over a century.Screen plugging and impairments by formation fines,scaling and corrosion cost oil and gas industry significant amount of resources.This study presents a detailed study on the corrosion and plugging of slotted liner,wire wrap screen and mesh screen samples extracted from the field to better understand some of the mechanisms for these poor field performances.Three types of standalone screen were received from operating wells to study the failure mechanism of the screen and provide recommendations for recompletion.A thorough visual inspection of all screens was performed and documented in this paper.From the results of the visual inspection a certain section of each screen was cut for further detailed microscopic study to better understand the scaling and plugging mechanism,as well as microscopic geometry of the plugged and corroded zone.The results highlighted the importance of the corrosion in the base pipe on the observed performances.All the studies pointed toward the flow dependence corrosion behavior,and the role of the water cut on the corrosion rate.The wire wrap screens have been in service for less than a year,yet the extensive corrosion led to creation of several holes in the pipe.The study showed the corrosion initiated from inside the pipe.Similarly,the corrosion of the slotted liner samples showed a strong flow dependent corrosion rate,where the corrosion rate on the slot/formation interface was slightly higher.The mesh screen showed very high plugging percentage by formation fines,where a thick film of clay and fine sand covered the space between the mesh and the base pipe.The results indicated that an inappropriate design of the mesh and pore could cause significant plugging.This paper provides several field examples of the corrosion and plugging of the standalone screens.The results could help engineer to better understand the risk of corrosion and plugging on the standalone screen design.This paper provides some general guidelines for assessing the scaling and corrosion potential at field condition based on the results of the screens studied in the paper.
机译:独立屏幕已被广泛用作石油行业的沙子控制解决方案超过一个世纪。通过形成罚款,缩放和腐蚀成本油和天然气行业的屏幕堵塞和损伤大量资源。本研究提出了对腐蚀和堵塞的详细研究从现场提取的槽内衬垫,丝网包装屏幕和网状屏幕样本,以更好地了解这些差的场景的一些机制。从操作井上收到了独立的独立屏幕,以研究屏幕的故障机制并为其提供建议重新完成。在本文中进行并记录了所有屏幕的彻底目视检查。从目视检查的结果,将每个屏幕的某个部分被切割用于进一步详细的微观研究,以更好地了解缩放和堵漏机构,以及显微镜插入和腐蚀区域的几何形状。结果强调了Corros的重要性在底管上的离子对观察到的性能。所有的研究指向流动依赖性腐蚀行为,以及水切割腐蚀速率的作用。丝网纸盒已在不到一年内使用不到一年,但很广泛腐蚀导致在管道中产生几个孔。研究表明,从管内部发起的腐蚀。相似的腐蚀,开槽衬里样品的腐蚀显示出强大的流动依赖性腐蚀速率,其中槽/地层界面上的腐蚀速率是略高。网眼筛网通过形成细粒显示出非常高的堵塞百分比,其中粘土和细砂的厚膜覆盖了网状物和基管之间的空间。结果表明网状物和孔隙的不恰当设计可能导致重要意义插头。这篇论文提供了独立屏幕腐蚀和堵塞的几个现场示例。结果可以帮助工程师更好地理解腐蚀和插头的风险在独立屏幕设计上。本文提供了一些基于本文中研究的屏幕的结果评估现场条件下的缩放和腐蚀潜力的一般指南。

著录项

相似文献

  • 外文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号