首页> 外文会议>Corrosion Annual Conference and Exposition >STRESS CORROSION CRACKING OF A COLD WORKED 22Cr DUPLEX STAINLESS STEEL PRODUCTION TUBING IN A HIGH DENSITY CLEAR BRINE CaCl_2 PACKER FLUID--Results of the Failure Analysis at Deep Alex and Associated Laboratory Experiments
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STRESS CORROSION CRACKING OF A COLD WORKED 22Cr DUPLEX STAINLESS STEEL PRODUCTION TUBING IN A HIGH DENSITY CLEAR BRINE CaCl_2 PACKER FLUID--Results of the Failure Analysis at Deep Alex and Associated Laboratory Experiments

机译:高密度透明盐水CaCl_2包装液中冷轧22Cr双相不锈钢生产管的应力腐蚀开裂 - 深度亚历克斯和相关实验室实验失效分析的结果

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The Deep Alex well was a gas well in the Gulf of Mexico with a bottom hole temperature of 370 deg F (188 deg C) and pressure of 16,800 psi (116 MPa). The gas contained H_2S at a maximum partial pressure of 0.25 psi (1.7 kPa) and CO_2 partial pressure of 672 psi (463 kPa), i.e., at bottomhole. The well was completed with a 22Cr duplex stainless steel (UNS S31803) that had been cold drawn to a minimum yield of 125 ksi (862 MPa). The production environment was within the environmental limits established in-house for this 22Cr duplex stainless steel. The use of the tubing and its properties also complied with NACE MR0175. The annular completion fluid was 11.0 ppg CaCl_2 that contained an oxygen scavenger and high temperature inorganic corrosion inhibitor; the contents of additives at the time of well completion were not stated. After one month of production of gas from the Deep Alex well in late 1999, the production tubing failed, forcing the well to be shut-in. No one was injured and no harm to the environment occurred because of the failure or subsequent operations to control the well. A failure analysis and subsequent laboratory program demonstrated that the cause of the failure was environmentally assisted cracking of the 22Cr duplex, a direct result of the production of H_2S by the decomposition of the sodium thiocyanate corrosion inhibitor in the CaCl_2 completion fluid in the annulus.
机译:Deep Alex井是墨西哥湾的气体井,底部孔温度为370°F(188℃)和16,800psi的压力(116MPa)。气体含有H_2S,最大部分压力为0.25psi(1.7kPa)和672psi(463kPa)的Co_2分压,即在底部。该孔用22Cr双相不锈钢(未S31803)完成,冷却至最低产率为125 kSi(862MPa)。生产环境是该22Cr双相不锈钢建立的环境限制范围内。使用管道及其性质也符合NACE MR0175。环形完成液为11.0ppg CaCl_2,其含有氧清除剂和高温无机腐蚀抑制剂;未陈述井完成时添加剂的含量。在1999年底,从深度亚历克斯生产的一个月生产的气体后,生产管道失败,强迫井关闭。由于失败或随后的操作来控制井,没有人受伤,对环境没有伤害。失败分析和随后的实验室方案证明了失败的原因是22Cr双链体的环境辅助开裂,通过在环空中的CaCl_2完成液中的硫氰酸钠腐蚀抑制剂分解的直接结果。

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