首页> 外文会议>Middle East Drilling Technology Conference Exhibition >Dynamic Underbalanced Perforating System Increases Productivity and Reduces Cost in East Kalimantan Gas Field:A Case Study
【24h】

Dynamic Underbalanced Perforating System Increases Productivity and Reduces Cost in East Kalimantan Gas Field:A Case Study

机译:动态卧间穿孔系统提高了生产率并降低了东康马坦天然气场的成本:案例研究

获取原文

摘要

New gas wells at Tunu field in East Kalimantan are normally perforated using the extreme underbalanced(EUB)technique, in which a large static pressure differential between the wellbore and formation,or initial underbalance,is set before the gun is fired.This requires an operation to unload wellbore liquid,a wireline operation to set an anchoring tool,and several slickline operations to run and retrieve the gun string. The required degree of underbalance depends primarily on rock properties such as permeability,porosity,and strength. A new approach produces a well dynamic underbalance (the transient underbalance just after creating the perforation cavity).By basing the job design on the properties of the reservoir,wellbore,and gun string,the technique consistently minimizes perforation damage and thus maximizes productivity.This technique is based on recent single-shot perforating experiments that show that it is the maximum dynamic underbalance-not the initial underbalance-that governs perforation cleanup.The wellbore pressure was found to vary considerably during the first half-second after the charges were detonated.This variation in wellbore pressure can be manipulated to give a large dynamic underbalance. Perforating with the new technique and electric wireline was performed on 10 wells in the field.Software that considered wellbore geometry,fluid,gun-string selection,and reservoir properties was used to design a specific gun-string configuration and to predict the productivity increase contributed by the underbalance.The jobs were performed smoothly with significant cost savings compared to conventional EUB operations and yielded an increased productivity.Details of the perforating jobs with the new technique will be described,including a cost reduction of approximately 40%and a significant production increase. Testing revealed an average skin value for four wells of-0.29, versus the average skin of 4.73 from 35 conventional EUB perforating jobs executed during the multi-year interval from 2000 to 2004.
机译:隧道隧道在东卡马丹隧道的新煤气井通常使用极端的欠平衡(eub)技术穿孔,其中在枪发射之前设定了井筒和地层之间或初始损价之间的大静压差异。这需要一个操作要卸载井筒液体,有线操作以设置锚定工具,以及运行的几个Slickline操作,并检索枪弦串。所需程度的产高程度主要取决于岩石性质,如渗透性,孔隙率和强度。一种新方法产生了一种良好的动态余量(在创建穿孔腔之后的瞬态百分比)。基于储层,井筒和枪支串的性质基础设计,该技术始终如一地减少穿孔损伤,从而最大限度地提高生产率。这技术是基于最近的单次穿孔实验,表明它是最大动态衰退 - 而不是初始不平衡 - 控制穿孔清理。在引爆电荷后,井眼压力在前半秒后变化很大。可以操纵这种井筒压力的这种变化以产生大的动态减少。通过新技术和电线线进行穿孔,在野外的10个井上进行。用于考虑井筒几何形状,流体,枪弦串选择和储层属性的软件来设计特定的枪弦串配置,并预测生产率增加通过不平衡。与传统的EUB操作相比,作业与常规成本相比,并产生了增加的生产力。将描述具有新技术的穿孔作业的产品,包括降低约40%和显着的产量增加。测试显示了四个井的平均皮肤值为0.29,而与2000年至2004年的多年间隔中的35个常规EUB穿孔作业的平均皮肤为4.73。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号