首页> 外文会议>2005 SPE international improved oil recovery conference in Asia Pacific >Dynamic Underbalanced Perforating System Increases Productivity and Reduces Costin East Kalimantan Gas Field: A Case Study
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Dynamic Underbalanced Perforating System Increases Productivity and Reduces Costin East Kalimantan Gas Field: A Case Study

机译:动态不平衡射孔系统在东加里曼丹气田提高生产率并降低成本:一个案例研究

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New gas wells at Tunu field in East Kalimantan are normallyrnperforated using the extreme underbalanced (EUB) technique,rnin which a large static pressure differential between thernwellbore and formation, or initial underbalance, is set beforernthe gun is fired. This requires an operation to unload wellborernliquid, a wireline operation to set an anchoring tool, andrnseveral slickline operations to run and retrieve the gun string.rnThe required degree of underbalance depends primarily onrnrock properties such as permeability, porosity, and strength.rnA new approach produces a well dynamic underbalancern(the transient underbalance just after creating the perforationrncavity). By basing the job design on the properties of thernreservoir, wellbore, and gun string, the technique consistentlyrnminimizes perforation damage and thus maximizesrnproductivity. This technique is based on recent single-shotrnperforating experiments that show that it is the maximumrndynamic underbalance—not the initial underbalance—thatrngoverns perforation cleanup. The wellbore pressure was foundrnto vary considerably during the first half-second after therncharges were detonated. This variation in wellbore pressurerncan be manipulated to give a large dynamic underbalance.rnPerforating with the new technique and electric wirelinernwas performed on 10 wells in the field. Software thatrnconsidered wellbore geometry, fluid, gun-string selection, andrnreservoir properties was used to design a specific gun-stringrnconfiguration and to predict the productivity increaserncontributed by the underbalance. The jobs were performedrnsmoothly with significant cost savings compared tornconventional EUB operations and yielded an increasedrnproductivity. Details of the perforating jobs with the newrntechnique will be described, including a cost reduction ofrnapproximately 40% and a significant production increase.rnTesting revealed an average skin value for four wells of -0.29, versus the average skin of 4.73 from 35 conventional EUBrnperforating jobs executed during the multi-year interval fromrn2000 to 2004.
机译:东加里曼丹省Tunu气田的新气井通常采用极端欠平衡(EUB)技术打孔,在开火之前先在井眼与地层之间设置一个较大的静压差,即初始不平衡。这需要卸载井眼液体的作业,需要设置锚固工具的电缆作业以及要运行和取回枪管的几条钢丝作业.rn所需的不平衡度主要取决于岩心的性质,例如渗透率,孔隙度和强度.rn一种新方法产生了动态良好的失衡(刚好在形成孔洞之后出现的瞬时失衡)。通过根据储层,井眼和枪管的属性进行作业设计,该技术始终能最小化射孔损伤,从而最大限度地提高生产率。该技术基于最近的单发射孔实验,该实验表明,控制射孔清理的是最大动态失衡而不是初始失衡。在引爆装药后的前半秒内,发现井眼压力变化很大。可以控制井眼压力的这种变化,以产生较大的动态欠平衡。rn在新技术中进行射孔,并在现场对10口井进行了电缆测井。考虑井眼几何形状,流体,枪管选择和储层特性的软件用于设计特定的枪管配置并预测由欠平衡造成的生产率提高。与常规EUB操作相比,这些工作顺利进行,节省了大量成本,并提高了生产率。将描述使用新技术的射孔作业的详细信息,包括降低成本约40%和显着提高产量。rn测试显示,四口井的平均表皮值为-0.29,而执行的35个常规EUB的平均表皮值为4.73。从2000年到2004年的多年间隔。

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