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Pioneering 'Gate Valve Milling' Operation Performed With Coiled Tubing Recovers an Important Oil Producer Offshore Brunei

机译:通过卷绕管道进行开拓“闸阀铣削”操作恢复了一个重要的石油生产商海上文莱

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Brunei Shell Petroleum offshore well A was offline and shut in due to the 3 1/8" 5K lower master valve on the monoblock tree, being seized in the closed position, due to scale production. The subsequent loss of production was 200 m3 (1260 BOPD), with a monetary value of US$1.5 million per month at $40 per barrel. Two options were considered for recovering the well using well intervention techniques rather than a complete workover and well killing operation. 1. Mobilize a "Gate Valve Milling Machine" the nearest being available was in Europe. 2. Mill the Gate Valve with a coiled tubing unit, which was already on the platform, performing a stimulation programme on adjoining wells. Option one was expensive due to high mobilization costs, some HSE issues, well control but this was a tried and test method of remedying the problem. Option two was a somewhat untried operation, which had only been performed as far as BSP and the contractors involved knew, once before in the North Sea. Given the coiled tubing unit was already on the platform, and the specialist low speed high torque motors with an anti stall device and specialist mills were availed in the time frame required. The decision process based on HSE, engineering review (SWOP), and cost considerations, chose the coiled tubing option. The paper will examine the problem with the wellhead master valve, the HSE, engineering and cost decision process leading up to the decision to go with the coiled tubing option. The milling operation from programme inception to successful execution of the milling operation, and placing the well back on line, will review in detail. Other operators will be able to benefit from this safe, low cost and time saving method of recovering production from wells with similar problems, which are many around the world.
机译:文莱壳牌石油公司海上油井A是离线和关闭在由于3 1/8" 5K下主对整块树阀,在关闭位置被抓住,由于规模生产。生产的随后损失是200立方米(12​​60桶石油当量),与在每桶40 $ US $ 150万货币价值每月。考虑两个选项用于恢复以及用修井技术,而不是一个完整的修井和压井作业。1.动员“闸阀铣床”最近的是可用的是在欧洲。2.磨闸阀具有连续油管单元,这是已经在该平台上,在相邻的井进行刺激计划。选项之一是高动员成本,一些HSE问题,由于价格昂贵,以及控制但这是一个尝试和纠正问题的测试方法。方案二是有些未经试验的操作,这仅被尽可能BSP进行,涉及到的承包商北海知道,前一次。鉴于日È连续油管单元已经在平台上,并用抗失速设备和专家磨机专科低速高扭矩电机在所需的时间帧被availed。基于HSE的决策过程,工程审核(SWOP),和成本的考虑,选择了连续油管选项。本文将探讨与井口主阀时,HSE,工程和价格决策过程导致对决定使用连续油管选项的问题。从计划以来,铣削操作,铣削操作的成功执行,并把上线靠后,将详细审查。其他运营商将能够从这种安全,成本低,节省时间从类似的问题,这是世界各地的许多油井恢复生产方法中获益。

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