首页> 外文会议>2005 SPE annual technical conference and exhibition (ATCE 2005) >Pioneering 'Gate Valve Milling' Operation Performed With Coiled Tubing Recovers anImportant Oil Producer Offshore Brunei
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Pioneering 'Gate Valve Milling' Operation Performed With Coiled Tubing Recovers anImportant Oil Producer Offshore Brunei

机译:连续油管的开创性“闸阀铣削”操作可回收重要的产油国文莱

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Brunei Shell Petroleum offshore well A was offline andrnshut in due to the 3 1/8" 5K lower master valve on thernmonoblock tree, being seized in the closed position, duernto scale production. The subsequent loss of productionrnwas 200 m3 (1260 BOPD), with a monetary value ofrnUS$1.5 million per month at $40 per barrel.rnTwo options were considered for recovering the wellrnusing well intervention techniques rather than arncomplete workover and well killing operation.rn1. Mobilize a "Gate Valve Milling Machine" the nearestrnbeing available was in Europe.rn2. Mill the Gate Valve with a coiled tubing unit, whichrnwas already on the platform, performing a stimulationrnprogramme on adjoining wells.rnOption one was expensive due to high mobilizationrncosts, some HSE issues, well control but this was a triedrnand test method of remedying the problem. Option twornwas a somewhat untried operation, which had only beenrnperformed as far as BSP and the contractors involvedrnknew, once before in the North Sea.rnGiven the coiled tubing unit was already on the platform,rnand the specialist low speed high torque motors with anrnanti stall device and specialist mills were availed in therntime frame required. The decision process based onrnHSE, engineering review (SWOP), and costrnconsiderations, chose the coiled tubing option.rnThe paper will examine the problem with the wellheadrnmaster valve, the HSE, engineering and cost decision process leading up to the decision to go with the coiledrntubing option. The milling operation from programmerninception to successful execution of the millingrnoperation, and placing the well back on line, will reviewrnin detail.rnOther operators will be able to benefit from this safe, lowrncost and time saving method of recovering productionrnfrom wells with similar problems, which are many aroundrnthe world.
机译:文莱壳牌石油公司的海上油井A处于离线状态,这是由于在rnonemonoblock树上的3 1/8“ 5K下主阀处于关闭位置,由于规模生产而被关闭。随后的生产损失为200 m3(1260 BOPD),货币价值为每月150万美元,每桶40美元。rn考虑了两种选择来恢复使用井眼干预技术而不是完全的修井和压井作业。rn1。动员“门式阀门铣床”在欧洲最接近。 rn2。用盘管装置碾压闸阀,该装置已经在平台上,在相邻的井上执行增产计划。方案一由于动员成本高,一些HSE问题,井控制而昂贵,但这是补救方案选项tworn是一个未经尝试的操作,直到BSP和涉及的承包商才进行,直到以前北海。鉴于连续油管装置已经在平台上,因此在需要的时间范围内配备了带有nranti失速装置的专业低速高扭矩电机和专业轧机。基于HSE,工程审查(SWOP)和成本考虑的决策过程选择了连续油管选项。本文将研究井口主阀,HSE,工程和成本决策过程的问题,最终决定采用连续油管。选项。从程序员开始到成功执行铣削操作的铣削操作,然后将其重新投入生产,将进行详细审查。其他操作员将能够从这种安全,低成本和省时的方法中受益,该方法可从存在类似问题的井中恢复生产。世界各地的许多人。

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