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Successful Application of Non-Intrusive Solids Detection Monitor in High Rate Gas wells

机译:在高速速率气井中的非侵入式固体检测监测仪的成功应用

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Solids production problems in the petroleum industry are well documented and several effective methods have been developed over the years to alleviate these problems. These issues become more costly and disastrous when dealing with high rate sour gas wells. Uncontrolled solids production in these types of wells can lead to choke cut-outs, eroded flowlines and damaged production facilities. Under conditions of high pressures and high rates, the ability to determine the solids production and controlling it is of paramount importance for reasons of safety, protection of the environment and the asset plus the attendant economic considerations. Solids monitoring was attempted during the first phase of Saudi Aramco’s first offshore Non- Associated Gas (NAG) field operations.. However the monitoring equipment failed to detect large particulates during the clean-up operations resulting in erosion of some of the choke trims. Fortunately, upon inspection there was no damage to the choke bodies or flowlines. These solids detectors were used on one well together with the Solids Management System (SMS) utilized for cleaning up the wells to 50 MMSCFD with the rig on location to confirm its ability to measure the solids production. For the second phase of operations, the solids detectors were recalibrated based on the previous findings and lessons learnt. The experience proved invaluable in the wells’ ramp-up operations, which were completed safely and without incidents. This paper describes the process and procedures employed in the ramping up operations of the wells to 120 MMSCFD without adversely affecting the production surface facilities. Furthermore, the lessons learnt and enhancements to the solid detectors resulting in the successful implementation are presented. This is the first time in the industry that these non-intrusive monitoring devices have been used successfully for this type of application.
机译:石油工业的固体生产问题已良好记录,多年来已经开发了几种有效的方法,以减轻这些问题。在处理高速酸性气井时,这些问题变得更加昂贵和灾难性。这些类型的井中的不受控制的固体生产可以导致扼流带,侵蚀的流动线和损坏的生产设施。在高压和高速率的条件下,由于安全,保护环境和资产,以及服务员的经济考虑,确定固体生产和控制的能力至关重要。在沙特阿美公司的第一个海上无关气体(NAG)现场操作的第一阶段尝试了固体监测。然而,监测设备在清理操作期间未能检测大型颗粒,导致一些扼流修剪的腐蚀。幸运的是,在检查时,扼流体或流动线没有损害。这些固体探测器在一个良好的良好用上使用用于用钻机清理到50 MMSCFD的固体管理系统(SMS),以确认其测量固体产生的能力。对于第二阶段的操作,基于先前的发现和经验教训来重新校准固体探测器。在井中的速率运营中证明了这一经验,这是安全的,没有事件完全完成。本文介绍了井中升温运算的过程和程序,以120 mmscfd,而不会对生产表面设施产生不利影响。此外,介绍了对导致成功实现的固体检测器的经验教训和增强。这是行业中的第一次,即这些非侵入式监控设备已成功用于此类应用程序。

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