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On-site replacement of OLTC, drying of winding insulation, induced voltage test with PD measurement of 250 MVA, 400/110 kV, 40 year old transformer

机译:现场更换OLTC,卷绕绝缘干燥,诱导电压测试,PD测量为250 MVA,400/110 kV,40岁的变压器

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The On-Load Tap Changer (OLTC) was damaged beyond repair, but winding insulation has not been significantly aged in 250 MVA, 400 kV network transformer, despite more than 40 years of service. The transformer maker does not manufacture his type of OLTC anymore, and it was replaced by MR equivalent. To determine the winding-insulation condition induced-voltage test was performed up to 110% U_n, by energizing the tertiary winding from mobile motor-generator set operating at a higher frequency. Insulation of 400 kV winding revealed Partial Discharge (PD) level between 1200 and 1800 pC but no specific PD source was identified. Water content in the winding insulation amounted to 1.1% prior to the OLTC replacement. Very compact design of the tank required an assessment of dielectric stress around the leads from tap-winding to the tap-selector. These leads had to be extended, and clamping the joints and wrapping tape insulation in the cramped space required highly skilled craftsmen. The single access porthole has been sealed when no people were inside the tank, to limit ingress of air. An internal polymeric-membrane was installed inside the tank to separate the working area from the windings, where a small overpressure was kept with synthetic dry-air. Despite such precautions some moisture was absorbed by the winding-insulation surface during the OLTC replacement. To dry this insulation the transformer was heated by filling the tank with new oil warmed up by 65°C, then draining the oil and lowering the pressure to less than 1 Tor (133 Pa) for 24 hours. The moisture was extracted from the insulation outer-layers and lower than 1% content was measured using RVM and PDC methods, which are sensitive to the moisture trapped in the insulation surface, and to the moisture averaged over the whole insulation-volume, respectively. The induced-voltage test was repeated after completion of the OLTC replacement, and PD level in 400 kV winding insulation was reduced by an order of magnitude, and DGA indicated content of Hydrogen 3.5 ppm, Methane 0.35 ppm and no Acetylene. The transformer was put in service after 72 hour trial run. The successful on-site OLTC replacement in the large transformer manufactured in Japan 40 years ago confirmed feasibility of such operation. This meticulously prepared on-site operation, highly skilled engineers and technicians, as well as advanced instruments to assess the winding-insulation condition were the essential factors to extend the technical life of this strategically important and costly transformer.
机译:尽管超过40多年的服务,那么载有载变频器(OLTC)损坏,但卷绕绝缘在250辆MVA,400千伏网络变压器中尚未显着老化。变压器制造商不再制造了他的OLTC类型,并且它被同等议员所取代。为了确定绕组绝缘条件感应 - 电压测试通过在更高频率下操作的移动电动机发生器集中的三级绕组来进行高达110%U_N。 400 kV绕组的绝缘显示1200和1800pc之间的局部放电(Pd)水平,但没有识别出特定的PD源。在OLTC更换之前,卷绕绝缘中的含水量为1.1%。非常紧凑的罐设计需要评估介电应力,从引线周围从绕组到敲击选择器。这些引线必须延长,并夹紧在狭窄的空间中的接头和包裹带绝缘,所以高技能的工匠。当没有人在坦克内部时,单个接入孔孔已被密封,以限制空气的入口。将内部聚合物膜安装在罐内,以将工作区域与绕组分离,其中小过压与合成的干燥​​空气保持。尽管采取了这样的注意事项,但在OLTC更换期间,卷绕绝缘表面吸收了一些水分。为了干燥这种绝缘材料,通过将罐加热,用新的油加热65℃,然后将油降低并将压力降低至小于1(133Pa),以填充罐。使用RVM和PDC方法从绝缘外层中提取水分,并且使用RVM和PDC方法测量1%的含量,这些方法对捕获在绝缘表面中的水分敏感,并且分别对整个绝缘体积的湿度平均。在OLTC置换完成后重复诱导电压试验,并且400kV绕组绝缘中的PD水平减少了幅度,DGA表示的氢3.5ppm,甲烷0.35ppm和无乙炔。经过72小时的试运行后,变压器已投入使用。 40年前在日本制造的大型变压器中成功的现场OLTC更换确认了这种操作的可行性。这本精心准备的现场运营,高熟练的工程师和技术人员以及评估绕组绝缘条件的先进仪器是延长这一战略性重要性和昂贵的变压器技术寿命的基本因素。

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