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Innovative Solution Successfully Recompletes Problematic Well in Malaysia

机译:创新的解决方案在马来西亚成功地重新认识了问题

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An offshore operator in Malaysia had run a completion string in a highly deviated 7-in. gas well. When continuous pressure build-up in the production casing annulus was observed during well clean-up, leakage in the completion system was suspected. After several attempts to mitigate the pressure build-up failed, the operator initiated further investigation, which confirmed the suspicion. Small tubing leaks that were allowing produced gas inside the tubing to seep through to the annulus were found. These leaks could have allowed the pressure to increase, and possibly, could have caused the casing to collapse. In order to produce through the annulus, the pressure would have to be vented. With the high demand of gas in Malaysia and since the rig was still at the location, the project team decided to initiate immediate recompletion of the project instead of waiting for a later intervention. This well is one of three wells completed to develop the FN field within KCL area, located approximately 200 km offshore from Bintulu. The field was expected to deliver up to 100mmscf/day per well to help relieve an anticipated gas shortage. This paper discusses the history of the wells, the diagnostic methods used to analyze the well problems, the pros and cons of each solution considered, details regarding the recompletion chosen, and the challenges encountered during the recompletion activities. The discussion also highlights the successful solution used for closing and reopening the fluid loss isolation barrier valve (FLIBV) with a wireline tractor rather than with other options considered after conducting a successful system integration test (SIT) prior to the project execution. The unique solution chosen was a first for Malaysia, and probably, for the world. The success of the recompletion results provided improvements for future applications and will be a benchmark solution for future operations.
机译:马来西亚的离岸运算符在高度偏离的7英寸中运行了完成字符串。气井。当在良好的清理过程中观察到生产外壳环中的连续压力积聚时,怀疑完井系统的泄漏。经过几次尝试减轻压力累积失败,运营商发起了进一步的调查,证实了怀疑。发现,在管内允许产生气体的小型管泄漏被发现渗入环节。这些泄漏可能使压力增加,并且可能使壳体崩溃。为了通过环生产,必须发射压力。随着马来西亚的气体需求很高,由于钻机仍处于地点,项目团队决定立即开始重新完成项目,而不是等待后来的干预。这井是三个井中完成的井之一,以便在KCL地区开发FN字段,从宾鲁乌大约有200公里。该领域预计将提供高达100mMSCF /天,以帮助缓解预期的气体短缺。本文讨论了井的历史,用于分析井问题的诊断方法,考虑各种解决方案的利弊,有关选择的重新完成的细节,以及在重新完成活动期间遇到的挑战。讨论还突出了用于关闭和重新开放的成功解决方案,并使用有线拖拉机重新打开流体损耗隔离屏障阀(Flibv),而不是在项目执行之前进行成功的系统集成测试(SIT)之后考虑的其他选项。选择的独特解决方案是马来西亚的第一个,可能是世界。重新完成结果的成功提供了未来应用的改进,并将成为未来运营的基准解决方案。

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