首页> 外文会议>Combined Power Plant Air Pollutant Control Mega Symposium >Achieving NO{sub}x Emissions of Less Than 0.10 lb/mmBtu in a 600 MWe Tangentially Fired Boiler Burning PRB Coal Using Combustion System Modifications
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Achieving NO{sub}x Emissions of Less Than 0.10 lb/mmBtu in a 600 MWe Tangentially Fired Boiler Burning PRB Coal Using Combustion System Modifications

机译:在使用燃烧系统修改的600 MWE切向燃烧的锅炉中达到{Sub} x排放量小于0.10磅/ mmBtu

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In June 2001 the Lower Colorado River Authority (LCRA) entered into a competitively bid contract with ALSTOM Power Inc. (ALSTOM) to design, supply and install low NO{sub}x equipment for Fayette Power Project Units 1 and 2. The low NO{sub}x system was installed on Unit 1 during a fall 2002 outage. ALSTOM tuned the modified firing system during the contracted time period, achieving emissions that were lower than the contractual guarantees. After the Low NO{sub}x Concentric Firing System (LNCFS) was commissioned, LCRA continued to tune the boiler and further reduced NO{sub}x emissions. The capabilities of both the modified firing system and the existing control system have been utilized to minimize emissions, even while plant load varied. NO{sub}x emissions that resulted in a yearly average of 0.12 lb/mmBtu and monthly averages of less than 0.10 lb/mmBtu have been achieved. Fly ash Unburned Carbon (UBC) remained essentially unchanged from pre-retrofit levels, and Carbon Monoxide (CO) emissions of less than 200 ppm were also achieved.
机译:2001年6月,较低的科罗拉多河权威(LCRA)与Alstom Power Inc.(Alstom)签订了竞争力的竞标合同,以设计,供应和安装低{Sub} X设备,为Fayette Power项目1和2.低{Sub} X系统在2002年下降期间安装在单元1上。 Alstom在合同时间段期间调整了修改的射击系统,实现低于合同担保的排放。在低{Sub} x同心烧制系统(LNCFS)之后,LCRA继续调整锅炉,进一步减少NO {Sub} x排放。改进的射击系统和现有控制系统的能力已经利用来最小化排放,即使在植物负载变化时也是如此。没有{sub} x排放量为每年平均为0.12磅/ mmbtu和每月平均值的低于0.10磅/ mmbtu。粉煤灰未燃烧的碳(UBC)仍然基本不变地与预热剂水平保持不变,并且还达到了少于200ppm的一氧化碳(CO)排放。

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