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Slow-Roll of 40 MW Condensing-Extraction Steam Turbines in a 420 MW Cogeneration Plant

机译:420 MW热电联产厂中的40 MW冷凝式提取汽轮机的慢卷

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This paper describes efforts required to operate condensing-extraction steam turbine generators with flexible rotor design on a slow-roll (also called, true stand-by) mode of operation. This mode of operation became necessary as a result of changing steam demand from the refinery and the resulting decreased performance of the existing steam turbine generators and the associated economic losses for the cogeneration facility. Design modifications implemented to achieve slow-roll of steam turbine generators and produce maximum power output obtainable with new steam flow conditions without affecting reliability and availability of the entire cogeneration facility are discussed in this paper. Successful implementation of the proposed design approach was demonstrated through extensive field testing completed in the summer of 2011. A simple life cycle economic analysis shows that the payback period associated with the proposed design modifications implemented to two steam turbine generators at the plant is approximately six (6) months.
机译:本文介绍了在慢卷(也称为真正的备用)操作模式下使用柔性转子设计操作冷凝提取汽轮机发生器所需的努力。由于炼油厂的蒸汽需求改变蒸汽需求,因此,由于现有的汽轮机发生器的性能降低以及热电联产工具的相关经济损失,因此这种操作模式变得必要。实现的设计改进以实现蒸汽轮机发生器的慢卷,并产生最大功率输出,并在此纸张中讨论了新的蒸汽流动条件而不影响整个热电联产能力的可靠性和可用性。通过2011年夏天完成的广泛的现场测试证明了拟议的设计方法的成功实施。简单的生命周期经济分析表明,与厂房两种汽轮机发生器实施的建议设计修改相关的投资回收期大约是六个( 6个月。

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