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Process Alternatives to Recover High-Grade Iron Ore Concentrate from the Thickener Underflow Slimes of the Sishen Beneficiation Plant

机译:从苏什益植物植物的增稠剂下溢铁液中恢复高档铁矿石浓缩物的过程替代品

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Kumba Iron Ore's Sishen Mine is one of the world's largest iron ore mining operations situated in the Northern Cape, South Africa. It produces 29 million tonnes of iron ore products per annum using a Dense Medium Separation (DMS) beneficiation process. Kumba is currently commissioning the Sishen Expansion Project (SEP) which will produce a further 13Mtpa product through a jigging beneficiation process. The products from the Sishen Mine are highly sought after and consumed by domestic and various European and Asian customers. During beneficiation iron ore slimes are generated and discarded as waste material to the slimes dams. A study was initiated in 2005 to investigate processes to beneficiate these slimes to saleable products - prompted by the current high demand for iron ore products and the high grade in the Sishen slimes thickener underflow of approximately 54 percent Fe. Initial laboratory scale test work indicated that a 66.5 percent Fe iron ore concentrate could be produced from the Sishen slimes thickener underflow through a process of classification, two stage wet high intensity magnetic separation (WHIMS) and five stage flotation. This process, however, did not produce the desired results during pilot plant testing and numerous alternative process routes were investigated. The process that did achieve the desired product grade of 66.5 percent Fe at economically feasible product yields consisted of two stage WHIMS using SLON magnetic separators. Results achieved indicate that the thickener underflow slimes can be upgraded from 54 percent Fe to 66.5 percent Fe at a product yield of ca. 40 percent . Product yield could be increased through the further beneficiation of the SLON tails. The Sishen slimes thickener underflow production rate is ca. 3Mtpa - resulting in a potential concentrate production of ca. 1.2Mtpa. The slimes concentrate will be fed to a pelletising plant that will produce 66 percent Fe pellets destined for domestic and or export markets.
机译:Kumba Iron Ore's Sishen Lime是位于南非北开普敦的世界上最大的铁矿石开采业务之一。它使用致密介质分离(DMS)受益方法每年生产2900万吨铁矿石产品。 Kumba目前正在调试Sishen扩展项目(SEP),该项目将通过跳汰私人流程产生另外的13MTPA产品。苏珊矿的产品受到国内和各种欧洲和亚洲客户的追捧和消费。在酿酒渣中,在粘液坝的废料产生并丢弃铁矿石。在2005年开始研究,调查将这些酵母的流程进行促进,以销售产品 - 目前对铁矿石产品的高需求和苏什人的高档增稠剂欠下约54%的Fe。初始实验室规模测试工作表明,通过分类过程,两级湿高强度磁分离(突发)和五阶段浮选,可以从斯兰登粘液增稠剂底部生产66.5%的Fe铁矿矿剂。然而,此过程在试验工厂测试期间没有产生所需的结果,并研究了许多替代过程路线。在经济上可行的产品产量下达到所需产品级的方法,该过程由使用Slon磁性分离器的两级突发突发。实现的结果表明,增稠剂下溢液可以从54%的Fe升级到加利福的产品产率下降到66.5%Fe。 40%。通过Slon Teats的进一步优势可以增加产品产量。 Sishen Slimes增稠剂底部流量是CA。 3MTPA - 导致CA的潜在集中生产。 1.2MTPA。粘液浓缩物将被送入颗粒化植物,该植物将产生66%的Fe颗粒,用于国内和或出口市场。

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