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PRODUCTIVITY IMPROVEMENT AT A MANUFACTURING WORKSTATION THROUGH APPLICATION OF ERGONOMIC PRINCIPLES

机译:通过应用符合人体工程学原则,制造工作站的生产力改进

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An appliance manufacturer reported lack of productivity at a consumer freezer assembly line. The procedure of connecting tube while fixing the screws and turning the shell of the product on a repeated basis required continuous body movement along with high pressure to be applied by the operator. The goal of this project was to observe and evaluate instances of human machine interface which may result into significant stress on the shoulder and lower back and thereby improve the productivity of the workstation. Time study and ergonomic evaluation was conducted to find the frequency of each freezer being turned and to measure stress. Few alternative approaches were designed and recommended to the company. One of the suggestions required addition of an operator to lift the shell while another approach recommended application of job rotation principle. Results of this project and a discussion of a cost-effective approach to solve the problem are presented in this paper.
机译:家电制造商报告了消费者冰柜装配线缺乏生产力。在固定螺钉的同时连接管的步骤并在重复的基础上转动产品的外壳所需的连续体运动以及操作者施加高压。该项目的目标是观察和评估人机界面的情况,这可能导致肩部和腰部的显着应力,从而提高工作站的生产率。进行时间研究和符合人体工程学评价,以找到每个冰箱的频率转动并测量应力。为公司设计并推荐了很少的替代方法。其中一个建议需要添加操作员以抬起外壳,而另一种方法推荐使用作业旋转原理。本文介绍了该项目的结果和对解决问题的经济有效方法的讨论。

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