首页> 外文会议>30th annual national conference of the American Society for Engineering Management 2009 >PRODUCTIVITY IMPROVEMENT AT A MANUFACTURING WORKSTATION THROUGH APPLICATION OF ERGONOMIC PRINCIPLES
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PRODUCTIVITY IMPROVEMENT AT A MANUFACTURING WORKSTATION THROUGH APPLICATION OF ERGONOMIC PRINCIPLES

机译:通过采用人机工程学原理来提高制造工厂的生产率

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摘要

An appliance manufacturer reported lack of productivity at a consumer freezer assembly line. The procedure of connecting tube while fixing the screws and turning the shell of the product on a repeated basis required continuous body movement along with high pressure to be applied by the operator. The goal of this project was to observe and evaluate instances of human machine interface which may result into significant stress on the shoulder and lower back and thereby improve the productivity of the workstation. Time study and ergonomic evaluation was conducted to find the frequency of each freezer being turned and to measure stress. Few alternative approaches were designed and recommended to the company. One of the suggestions required addition of an operator to lift the shell while another approach recommended application of job rotation principle. Results of this project and a discussion of a cost-effective approach to solve the problem are presented in this paper.
机译:一家家电制造商报告说,消费者冰柜装配线的生产率不足。在固定螺钉的同时连接管并反复转动产品外壳的过程要求操作人员持续不断地移动身体并施加高压。该项目的目的是观察和评估人机界面的实例,这些实例可能导致肩膀和下背部承受巨大压力,从而提高工作站的生产率。进行了时间研究和人体工程学评估,以找到每个冷冻机的转动频率并测量压力。很少有替代方法被设计并推荐给公司。一项建议要求增加一名操作员来抬起壳体,而另一种方法则建议应用作业旋转原理。本文介绍了该项目的结果,并讨论了一种经济有效的方法来解决该问题。

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