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First Worldwide Successful Implementation of Coiled Tubing Compatible Novel Fiber Laden Diverter for Matrix Stimulation Using a New Generation High Rate Fiber Optic Real-Time Telemetry System

机译:首先全球成功实施卷管兼容新型纤维载带,用于使用新一代高速光纤实时遥测系统进行矩阵刺激

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The objective of this paper is to highlight first worldwide implementation of coiled tubing (CT) compatible self-degradable fiber laden diverter for matrix stimulation treatment using enhanced high rate fiber optic real time telemetry system. The self-degradable fiber laden diverter has been used in bullheading acid stimulation treatments aimed to maximize reservoir contact and enhance gas production. Recently, the physical properties of fiber has been re-engineered enabling them to be pumped down coiled tubing to enhance diversion and stimulation effectiveness. Coiled tubing with fiber optic real-time telemetry has been utilized for many years in Saudi Arabia for matrix stimulation treatments and well interventions as it provides real-time bottom-hole parameters such as pressure, temperature, casing collar locator, gamma ray, tension and compression as well as distributed temperature sensing (DTS) to optimize fluid placement. The successes achieved with previously used 2 1/8-in. bottom-hole assembly (BHA) for coiled tubing with real time telemetry system offered the maximum rate of 2.0 barrel per minute (bpm), whereas this rate became a limitation to achieve the desired fiber concentration for diversion when fiber laden fluids were used. The low rate provision by 2 1/8-in. BHA led to the need of a new generation high rate 3.25-in. BHA to be used for coiled tubing fiber optic real-time telemetry system that can enable higher pumping rates, help in achieving the desired fiber concentration. For the first time in Saudi Arabian Carbonate reservoir, the novel fiber laden diverter was used during matrix stimulation treatment through 180 ft. perforated interval with new generation 3.25-in. bottom hole assembly (BHA) for coiled tubing fiber optic real-time telemetry system. The DTS used with the new generation coiled tubing high rate fiber optic real-time telemetry system helped in pre- and posttreatment evaluation. After successful high pressure coiled tubing stimulation using self-degradable fiber laden diverter with visco-elastic surfactant based acid system, the well performance exceeded expectation. The encouraging result was achieved by uniform stimulation coverage throughout the long perforation interval. The operation also proved the feasibility of using the new generation of fiber optic real-time telemetry system in challenging environment.
机译:本文的目的是突出3个卷绕管(CT)兼容的自降低光纤载带,用于使用增强的高速速率光纤实时遥测系统进行卷材刺激处理的圈子刺激处理。自降脂纤维升起的分流器已被用于Bullhead酸刺激处理,旨在最大限度地提高储层接触和增强天然气生产。最近,已经重新设计了纤维的物理性质,使它们能够向下泵送卷绕管以增强导流和刺激效果。带有光纤实时遥测的盘绕管已在沙特阿拉伯多年来用于矩阵刺激处理和井干预,因为它提供了压力,温度,套管领定位器,伽马射线,张力和张力等实时底孔参数压缩以及分布式温度感测(DTS)以优化流体放置。以前使用的2 1/8 in实现的成功。用于卷绕管的底部孔组件(BHA),实时遥测系统提供每分钟2.0桶的最大速率(BPM),而这种速率变得有限,以实现当使用纤维载体流体时实现所需的纤维浓度。低速规定2 1/8英寸。 BHA导致了新一代高速率为3.25英寸。 BHA用于卷绕管道光纤实时遥测系统,可以实现更高的泵送速率,有助于实现所需的纤维浓度。在沙特阿拉伯碳酸盐储层中首次,在基质刺激处理期间通过180英尺的基质刺激处理使用了新型纤维升降机。具有新一代3.25英寸的穿孔间隔。用于盘绕管道光纤实时遥测系统的底部孔组件(BHA)。 DTS与新一代卷绕管高速率光纤实时遥测系统有助于预处理评估。在成功的高压盘管刺激刺激通过具有粘性表面活性剂基酸系统的自降级纤维升起的分流器,井的性能超出了预期。通过在整个长穿孔间隔内均匀的刺激覆盖率来实现令人鼓舞的结果。该操作还证明了在挑战环境中使用新一代光纤实时遥测系统的可行性。

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