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Elimination of flow-induced pulsations and vibrations in a process installation - A combination of on site measurements, calculations and scale modeling

机译:在过程安装中消除流动诱导的脉动和振动 - 在现场测量,计算和规模建模上的组合

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The aim of the work described in this paper was to trace and eliminate vibration sources in a low pressure system with high flow velocities. Considerable vibration on the pipe system between a flashing vessel (6.5m diameter) and heat-exchangers resulted in fatigue failure, leakage and subsequent shut down of a chemical production plant. As compressors or pumps were not directly involved in the process, we considered aero-acoustic pulsations as the main cause of the high vibration levels. Analysis of the flow in the pipe system showed that mean flow velocities could rise up to 50m/s, which is rather high considering the speed of sound in the gas of 195ms/s. Furthermore separation of the flow from the pipe wall occurs at the outlets of a flashing vessel, which resulted in estimated flow velocities of over 100m/s in the vena contracta. This paper provides an overview of the analysis done by a one-dimensional acoustical model and scale modeling of part of the piping. The recommended modification consists of a perforated pipe section between the outlets of the vessel and has been tested in a scale model. Tests have been performed with airflow at identical Mach numbers for different configurations with perforation ratios form 70 to 36%. The modification with a perforation ratio of 70% shows a reduction of a factor 5 of the pressure pulsation and vibration levels over the entire frequency range. The net pressure loss for this configuration is similar to that in the original lay-out without the perforated tube. This modification was implemented during a plant shutdown and proved to be very effective. The results are well in line with the predicted levels and on the basis of this success a similar design has been planned for two new installations.
机译:本文中描述的工作的目的是追踪和消除具有高流速的低压系统中的振动源。在闪光容器(直径6.5米)和热交换器之间的管道系统上的相当大的振动导致疲劳失效,泄漏和随后关闭化学生产植物。随着压缩机或泵未直接参与该过程,我们认为航空声脉动作为高振动水平的主要原因。管道系统中的流量分析表明,平均流速可升到50米/秒,这考虑到195ms / s气体的声速相当高。此外,从管壁中的流动发生在闪蒸容器的出口处,这导致静脉内的估计流速超过100m / s。本文概述了通过一维声学模型和一部分管道的规模建模完成的分析。推荐的修改包括在血管的出口之间的穿孔管部分,并且已经在比例模型中进行了测试。已经在相同的马赫数处进行了测试,用于不同的配置,穿孔比例为70%至36%。穿孔比为70%的修改示出了在整个频率范围内的压力脉动和振动水平的倍数5的减小。这种配置的净压力损失与未穿孔管的原始布局中的净压力损失类似。该修改是在工厂关闭期间实施的,并证明是非常有效的。结果符合预测的水平,并在此成功的基础上,为两个新安装计划了类似的设计。

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