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A Case History of Nitrogen Injection Monitoring in Rich Recycled Gas Condensate Reservoir, Onshore Gas Field, Abu Dhabi, UAE

机译:富含回收气体凝结水库中氮注射监测的案例历史,陆上气田,阿布扎比,阿联酋

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A mixture of Nitrogen and hydrocarbon gas was used as a cycling gas in a large rich gas condensate reservoir to maintain reservoir pressure and thus prevent condensate drop-out due to pressure decrease below the dew point pressure. The objective of using Nitrogen gas is to partially replace some of hydrocarbon injection gas, which has a high demand for Abu Dhabi domestic consumption. This paper presents the plan, implementation, results and analysis of an intensive reservoir monitoring program, which was conducted to monitor the Nitrogen injection and production. Additionally, the paper discusses lessons learned from the Nitrogen injection, inferences reached, and corrective actions taken. The Nitrogen injection was started as a Mixed Case (MC) injection, where a mixture of Nitrogen (~20%) and hydrocarbon gas (~80%) was injected in all existing injectors across the entire reservoir for a period of three years. The plan was to stop the MC injection and apply a Pure Case injection (PC), which consists of injecting only pure Nitrogen in the North West area of the reservoir. The objective of the PC injection is to localize the Nitrogen injection to be able to apply Nitrogen removal technology in a specific part of the existing surface facilities whenever high Nitrogen production is reached. Monitoring the Nitrogen production relies mainly on an intensive gas composition sampling and analysis, which have been conducted quarterly for all gas producers, in addition to other surveillance activities of the intensive reservoir monitoring program. The Nitrogen monitoring results and analysis of the MC injection showed Nitrogen breakthrough in many wells with increasing Nitrogen production trends. Different analytical techniques were applied to evaluate and predict the Nitrogen breakthroughs. Due to the unavailability of surface Nitrogen removal facilities and the increase in Nitrogen production during the MC injection, a Nitrogen risk assessment study supported a recommendation to stop the MC injection and continue cycling with dry hydrocarbon gas only as before. Also, it was decided to delay the planned PC injection for more evaluations and studies.
机译:氮气和烃气体的混合物用作大型富含气体冷凝水储存器中的循环气体,以保持储层压力,从而防止由于露点压力以下的压力降低而下降。使用氮气的目的是部分替代一些碳氢化合物注射气体,这对阿布扎比国内消费具有很大的需求。本文介绍了强化水库监测计划的计划,实施,结果和分析,该计划进行了监测氮气注射和生产。此外,本文讨论了从氮气注射液中学到的经验教训,达到的推论以及采取的纠正措施。注入氮气开始作为混合大小写(MC)注射剂,其中氮(约20%)和烃类气体(〜80%)的混合物中的所有现有的喷射器中注入在整个贮存期限为三年。该计划是停止MC注射并涂抹纯案例注射(PC),这包括仅在水库西北地区注射纯氮。 PC注射的目的是定位氮气注射,以便只要达到高氮生产,就能够在现有表面设施的特定部分中施加氮气去除技术。监测氮气产量主要依赖于密集的气体成分采样和分析,除了强化水库监测计划的其他监视活动外,还针对所有天然气生产商进行了季度。 MC注射的氮监测结果及分析显示了许多井中氮素生产趋势的氮气突破。应用了不同的分析技术来评估和预测氮突破。由于表面氮气去除设施的不可用和MC注射过程中的氮气产生的增加,氮风险评估研究支持推荐,以阻止MC注射,并继续用干燥的碳氢化合物气体循环。此外,决定延迟计划的PC注入以获得更多的评估和研究。

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