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Teamwork plus Technology Equals Reduced Emissions, Reduced Energy Usage, and Improved Productivity for an Oil Production Facility

机译:Teamwork Plus技术等于降低的排放,降低能源使用,提高石油生产设施的生产力

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Suncor Energy Inc. developed a long term plan to expand production from its oil sands operation north of Fort McMurray, Alberta up to 500,000 to 550,000 barrels/day in 2010-2012, while reducing the per barrel energy usage, emissions, and long term production cost target to under C$10 per barrel. Current production has been increased to 225,000 barrels/day through the application of advanced technologies and an ongoing series of expansion projects. This paper is limited to the integration of an advanced control system project into the existing Steepbank Mine and Extraction Process Plant. The Extraction Process separates the raw oil called bitumen from the mined ore and is the largest energy user on the site. A control system and energy audit was conducted in the fourth quarter of 2000 to form the basis for the ongoing energy reduction and production improvement Advanced Control Project. The project consists of initiatives ranging from simple operating procedures to integrating the new control system into major process modifications. When performance of the new Extraction control system controls was evaluated against the original 2000 baseline, the overall production gain was 9% to 12% valued at C$44 million/year with an additional C$8.7 million/year reduction in hot process water.. The Advanced Control Project is part of a greater Extraction production improvement and energy reduction program returning a total 2001 production increase of C$104 million/year when evaluated against the 2000 baseline. At the end of 2002 the Extraction Unit team effort returned an additional production increase of C$140 million/year while reducing hot process water energy usage an additional C$2.5 million/year.
机译:Suncor Energy Inc.制定了长期计划,以扩大艾伯塔堡堡港的石油卫砂运营生产,2010 - 2012年艾伯塔堡的石油砂运营速度为500,000至55万桶/天,同时减少了每桶能源使用,排放量和长期生产每桶10美元的成本目标。目前的产量通过应用先进技术和一系列扩张项目,增加到225,000桶/天。本文仅限于将先进的控制系统项目集成到现有的Steepank矿山和提取过程工厂中。萃取过程将称为沥青的原油与开采矿石分离,是该地点上最大的能量用户。 2000年第四季度进行了控制系统和能源审计,以形成持续的能源减少和生产改进先进控制项目的基础。该项目包括从简单的操作程序到将新控制系统集成到主要过程修改中的举措。当对原始2000个基线进行评估的新提取控制系统控制的性能时,整体产量增益为9%至12%,在4400万美元/年内重视,额外的速度下降了870万美元/年。先进的控制项目是更大的提取生产改进和能量减少方案的一部分,返回2001年的2001年的产量增加1.04亿美元/年度,评估2000年基线。截至2002年底,提取单位队伍努力额外增加1.4亿美元/年的产量增加,同时减少热处理水能使用额外的250万美元/年。

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