首页> 外文会议>National Association of Corrosion Engineers Annual Conference Exposition >STRESS CORROSION CRACKING OF A COLD WORKED 22Cr DUPLEX STAINLESS STEEL PRODUCTION TUBING IN A HIGH DENSITY CLEAR BRINE CaCl2 PACKER FLUID;Results of the Failure Analysis at Deep Alex and Associated Laboratory Experiments
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STRESS CORROSION CRACKING OF A COLD WORKED 22Cr DUPLEX STAINLESS STEEL PRODUCTION TUBING IN A HIGH DENSITY CLEAR BRINE CaCl2 PACKER FLUID;Results of the Failure Analysis at Deep Alex and Associated Laboratory Experiments

机译:冷加工22Cr双相不锈钢生产管中的应力腐蚀开裂在高密度透明盐水CaCl2封装机中; Deep Alex和相关实验室实验中的失效分析结果

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The Deep Alex well was a gas well in the Gulf of Mexico with a bottom hole temperature of 370 deg F (188°C) and pressure of 16,800 psi (116 MPa). The gas contained H2S at a maximum partial pressure of 0.25 psi (1.7 kPa) and CO2 partial pressure of 672 psi (463 kPa), i.e., at bottomhole. The well was completed with a 22Cr duplex stainless steel (UNS S31803) that had been cold drawn to a minimum yield of 125 ksi (862 MPa). The production environment was within the environmental limits established in-house for this 22Cr duplex stainless steel. The use of the tubing and its properties also complied with NACE MR0175. The armular completion fluid was 11.0 ppg CaCl2 that contained an oxygen scavenger and high temperature inorganic corrosion inhibitor; the contents of additives at the time of well completion were not stated. After one month of production of gas from the Deep Alex well in late 1999, the production tubing failed, forcing the well to be shut-in. No one was injured and no harm to the environment occurred because of the failure or subsequent operations to control the well. A failure analysis and subsequent laboratory program demonstrated that the cause of the failure was environmentally assisted cracking of the 22Cr duplex, a direct result of the production of H2S by the decomposition of the sodium thiocyanate corrosion inhibitor in the CaCl2 completion fluid in the annulus.
机译:深度亚历克斯井是墨西哥湾的煤气井,底部孔温度为370°C(188°C),压力为16,800 psi(116mPa)。气体在最大分压的0.25psi(1.7kPa)和672psi(463kPa),即在井孔的CO 2分压下含有H 2。该孔用22Cr双相不锈钢(未S31803)完成,冷却至最低产率为125 kSi(862MPa)。生产环境是该22Cr双相不锈钢建立的环境限制范围内。使用管道及其性质也符合NACE MR0175。配弹完全液是11.0ppg CaCl2,其含有氧清除剂和高温无机腐蚀抑制剂;未陈述井完成时添加剂的含量。在1999年底,从深度亚历克斯生产的一个月生产的气体后,生产管道失败,强迫井关闭。由于失败或随后的操作来控制井,没有人受伤,对环境没有伤害。失败分析和随后的实验室方案证明了失败的原因是22Cr双链体的环境辅助开裂,通过在环空中的CaCl 2完成液中的硫氰酸钠腐蚀剂的分解中产生H2S的直接结果。

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