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Postbuckling failure of carbon-epoxy compression panels

机译:碳 - 环氧压缩板的出现失效

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The post-buckled failure of carbon/epoxy compression panels is studied experimentally and theoretically. Four different designs are considered each of which has significant post-buckled strength with a failure load more than twice the bucklingload. The mechanisms which can initiate failure through stiffener debonding, prior to imminent explosive collapse, are postulated, taking account of the buckled mode shape. The specific mechanism which leads to failure in each of the particular fourdesigns is identified from careful experiments with complete panels and also by suitably loading transverse strips cut from the panel to be tested. These component tests provide a quantitative guide to the magnitude of a stress resultant which will leadto de-bond initiation. This stress resultant can then be related to a compression failure load through an FE analysis of the post-buckled panel.
机译:通过实验和理论地研究碳/环氧压缩板的后扣失效。四种不同的设计被认为每个不同的设计具有明显的屈曲强度,故障负载超过扣荷载的两倍。在迫在眉睫的爆炸崩溃之前,通过加强筋剥离在爆炸崩溃之前,可以启动故障的机制,考虑到弯曲模式形状。从仔细的实验​​中鉴定出在每个特定的四个特定的四个人中的失败的具体机制,并且还通过完整的面板,并且通过从待测面板切割的适当加载横向条带。这些组分试验提供了将导致脱键启动的应力结果的大小的定量指南。然后,这种应力通过后扣面板的FE分析可以与压缩失效负载有关。

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