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THE INTRODUCTION AND ANALYSIS OF THE WORLD'S FIRST HIGH-TEMPERATURE RETROFIT PROJECT ON A SUBCRITICAL COAL-FIRED POWER UNIT

机译:亚临界燃煤电力装置世界上第一个高温改造项目的介绍与分析

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Global warming concerns have pushed coal-fired power plants to develop innovative solutions which reduce CO_2 emissions by increasing efficiency. While new ultra-supercritical units are built with extremely high efficiency, with Pingshan Ⅱ approaching 50% LHV[1], subcritical units with much lower efficiency are a major source of installed capacity. The typical annual average net efficiency of subcritical units in China is about 37% LHV, and some are lower than 35% LHV. Since the total subcritical capacity in China is about 350GW and accounts for over one third of its total coal-fired power capacity, shutting all subcritical units down is not practical. Finding existing coal-fired plants a cost-effective solution which successfully combines advanced flexibility with high efficiency and low emissions, all while extending service lives, has challenged energy engineers worldwide. However, the (now proven) benefits a high temperature upgrade offers, compared to new construction options, made this an achievement worth pursuing. After many years of substantial incremental improvements to best-in-class technology, this first-of-its-kind subcritical high temperature retrofit successfully proves that a technically and economically feasible solution exists. It increases the main and reheat steam temperatures from 538°C (1000°F) to 600°C (1112℉), and the plant cycle and turbine internal efficiencies are greatly improved. This upgrade 's greatest efficiency gains occur at low loads, which is important as fossil plants respond to renewable energy's increased grid contributions. These are combined with best-in-class flexibility, energy-savings, and technological advances, i.e., flue gas heat recovery technology and generalized regeneration technologies [4]. This project, the world's first high-temperature subcritical coal-fired power plant retrofit, was initiated in April 2017 and finished in August 2019. Performance reports created by Siemens and GE record unit net efficiency at rated conditions improved from 38.6% to 43.5% LHV. The boiler's lowest stable combustion load with operational SCR, without oil-firing support, was reduced from 55% to 19%. Substitution or upgrading of high-temperature components extended the lifetime of the unit by more than 30 years. At a third of the cost of new construction, this project set a high-water-mark for retrofitting subcritical units, and meets or supports the requisite attributes for Coal FIRST, Coal Plant of the Future, proposed bv the United States Department of Energy (DOE) in 2019 .
机译:全球变暖的担忧推动了燃煤发电厂开发创新解决方案,通过提高效率来减少CO_2排放。虽然新的超超超临界单位以极高的效率为基础,但具有平山Ⅱ接近50%LHV [1],较低效率的亚临界单位是安装容量的主要来源。中国亚临界单位的典型年平均净效率约为37%LHV,其中一些低于35%的LHV。由于中国的总亚临界能力约为350gW,占其总燃煤电力容量的三分之一,关闭所有亚临界单位并不实用。寻找现有的燃煤工厂具有成本效益的解决方案,该解决方案成功结合了高效率和低排放的先进灵活性,同时延长了服务生活,在全球挑战了挑战性的能源工程师。然而,与新的建筑选择相比,(现已被证明)受益于高温升级优惠,使这一成就值得追求。经过多年的大量增量改进,以级别的技术为准,这首先进行了一类亚临界高温改造成功证明了技术和经济可行的解决方案存在。它将主要和再加热蒸汽温度从538°C(1000°F)增加到600°C(1112°),大大提高了植物循环和涡轮机内部效率。这种升级最大的效率收益发生在低负荷下,这与化石厂响应可再生能源的增加的电网贡献很重要。这些与最佳灵活性,节能和技术进步相结合,即烟气热回收技术和广义再生技术[4]。该项目是世界上第一个高温亚临界燃煤电厂改造,于2017年4月开始,2019年8月成立。西门子和GE纪录股额定条件的绩效报告从38.6%提高到43.5%LHV 。锅炉的稳定燃烧载荷与操作SCR,没有燃油支撑,减少了55%至19%。替代或升级高温成分将单位的寿命延长30年以上。该项目的三分之一,该项目设定了一种高水位,用于改造亚临界单位,并满足或支持未来煤炭煤炭煤炭的必要属性,提出了美国能源部的BV( DOE)2019年。

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